TKOF ABORTED DUE TO ACFT EQUIP PROB.
Synopsis
TKOF ABORTED DUE TO ACFT EQUIP PROB.
Narrative
ON TKOF FROM SJT; #2 ENG OVERTEMPED. THE TKOF PROC AT THIS ARPT IS PWR SET AT BRAKE RELEASE. ABORTED TKOF SEQUENCE AND RECHKED DATA AND CYCLED ICE PROTECTION AND BLEED AIR TO ENSURE ALL SYS OFF/CLOSED. AGAIN; ON PWR APPLICATION; #2 ENG OVERTEMPED. TAXIED BACK TO GATE WHERE DISPATCH (PART 121 CARRIER) CANCELLED FLT. A MECH WAS SENT FROM DFW TO SJT ON THE NEXT FLT. UPON THE MECH'S ARR; HE UNCOWLED THE NACELLE AND INSPECTED ALL FITTINGS ON THE P- 3 LINE. HE ALSO INSPECTED THE ANTI-ICE/START BLEED VALVE. I ALSO VISUALLY INSPECTED P-3 LINE AND SAW A SPLIT IN THE LINE COVERING ABOUT 30 PERCENT OF THE DIAMETER. THE MECH AGREED WITH ME THAT THAT WAS IN ALL PROBABILITY THE PROB. THE MECH CALLED MAINT CTL AND WAS ADVISED THAT THE PART WAS ALREADY ON ITS WAY. THE ACFT HAD SPENT THE PREVIOUS NIGHT AT A MAINT HUB WITH A LARGE SPLIT IN THE 'DT' (DIFFERENCE IN TEMP BTWN #1 AND #2 ENGS). THE SPLIT WAS THERE BEFORE MAINT AND AFTER; THEREFORE; IT CAN BE CONCLUDED THAT THE PROB EXISTED PRE AND POST MAINT. THE RUPTURED DUCT WAS PLAINLY VISIBLE; IF THE ENG WAS UNCOWLED. A BLEED LEAK OF THAT MAGNITUDE WOULD; IN ALL PROBABILITY; HAVE CAUSED AN ENG FIRE INDICATION AND NECESSITATED AN ENG SHUTDOWN; SUBJECTING ALL TO UNNECESSARY SAFETY HAZARDS. IN CONCLUSION; MAINT SHOULD HAVE INVESTIGATED A HIGH 'DT' FURTHER AND SWAPPED THE PART OUT THE PREVIOUS NIGHT. THE OTHER OBVIOUS CONCLUSION IS PLAIN TO SEE.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.