SMA JUST OUT FROM ANNUAL HAS STUCK NOSE GEAR.
Synopsis
SMA JUST OUT FROM ANNUAL HAS STUCK NOSE GEAR.
Narrative
ACFT HAD JUST COMPLETED ANNUAL INSPECTION WHICH HAD BEEN DUE IN JULY. I WAS TO RETURN IT TO CUSTOMER'S BASE ARPT; ABOUT 20 MI AWAY. I NOTED IN LOGBOOK THAT ANNUAL WAS SIGNED OFF OCT/XX/93. AS DATE WAS SEP/XY/93 I THOUGHT THAT; TECHNICALLY; ACFT WAS NOT LEGAL TO FLY; BUT FIGURED NOTHING WOULD HAPPEN ON SUCH A SHORT FLT. TOOK OFF; FLT WAS UNEVENTFUL. ENTERED PATTERN AND DROPPED GEAR. MAINS POPPED INTO PLACE; PUMP CONTINUED TO RUN FOR ABOUT 10 SECONDS THEN BREAKER POPPED ON LNDG GEAR. I RECYCLED WITH SAME RESULTS. TRIED TO PULL OUT HAND PUMP BUT IT WAS STUCK. FINALLY; I SLOWED DOWN AND JERKED BACK ON YOKE AND THE G-LOADING POPPED NOSE GEAR IN PLACE AND I GOT A GREEN LIGHT. LANDED UNEVENTFULLY. ACFT WAS RETURNED TO MAINT SHOP AND WORN PARTS FOUND ON NOSE GEAR; A NON-LOCKING NUT WAS USED IN PLACE OF A FIBRE LOCK NUT AND THERE WAS ALMOST NO HYD PRESSURE PUSHING NOSE GEAR DOWN. INSPECTION OF NOSE GEAR (AT ANNUAL) WAS DONE BY A RELATIVELY INEXPERIENCED A&P WHO APPARENTLY NEEDS MORE SUPERVISION. IF GEAR HADN'T COME DOWN; I HAVE TO THINK WHAT THE FAA AND INSURANCE COMPANY WOULD HAVE DONE CONSIDERING THE POST-DATING OF THE ANNUAL; JUST TO GIVE THE GUY AN EXTRA FEW DAYS BEFORE HIS NEXT INSPECTION.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.