TKOF ABORTED WHEN DHC-8-I FO UNABLE TO ROTATE ACFT DURING TKOF PROC.
Synopsis
TKOF ABORTED WHEN DHC-8-I FO UNABLE TO ROTATE ACFT DURING TKOF PROC.
Narrative
ON THE TKOF ROLL FROM RWY 29 AT INTXN ROMEO AT EWR; THE FO BEGAN ROTATING THE CTL WHEEL AT THE 'V1; ROTATE' CALL. THE NOSEWHEEL WAS NOT COMING OFF THE GND AND THE CTL WHEEL FELT NOSE HVY. AT THIS POINT; THE PF CONTINUED TO APPLY BACK PRESSURE AND ROLLED IN NOSE UP TRIM TO LIGHTEN CTL FORCES. THE CTL FORCES REMAINED HVY. THE NOSEWHEEL STILL STAYED ON THE GND; AND THE TKOF CONFIGN WARNING HORN SOUNDED. WE BOTH CALLED FOR AN ABORT; AND WE BROUGHT THE ACFT TO A STOP. WE NARROWLY AVOIDED RUNNING OFF THE END OF THE RWY. AS OF THIS WRITING; NO PROBS HAVE BEEN FOUND WITH THE ACFT LOADING OR WITH THE ELEVATOR OR TRIM SYS. ALTHOUGH WE STOPPED THE ACFT ON THE RWY; WE COULD HAVE IMPROVED OUR SAFETY MARGIN BY THE FOLLOWING: 1) NOT USING AN INTXN FOR TKOF; 2) NOT TAKING OFF DOWNWIND; 3) EXTRA ALLOWANCE FOR A WET RWY. WE MET ALL APPLICABLE CRITERIA FOR TKOF; EVEN DOWNWIND AT AN INTXN ON A WET RWY. IN PARTICULAR; INTXN TKOFS ARE ENCOURAGED AT OUR COMPANY TO SAVE MONEY. WE DECIDED ON THIS TKOF TO AVOID A DELAY OF APPROX 1 HR TO USE RWY 4L; WHICH WOULD HAVE GIVEN AN ADDITIONAL 4000 FT OF RWY AND NO TAILWIND. IN HINDSIGHT; WE CUT OUR SAFETY MARGINS ONE BIT AT A TIME UNTIL WE HAD VERY LITTLE LEFT. I ALSO BELIEVE THE POLICIES THAT ALLOWED US TO MAKE THIS ATTEMPTED TKOF UNDER THESE CIRCUMSTANCES SHOULD BE EVALUATED. SUPPLEMENTAL INFO FROM ACN 290983: FORM A JUDGEMENT POINT OF VIEW; IN FUTURE; I WOULD PROBABLY ELECT TO ACCEPT THE DELAY AND ACCEPT A LONGER RWY FOR TKOF. ALSO; THE DECISION TO ABORT AFTER V1 IS NOT NATURAL; I.E.; IT IS INGRAINED IN US FROM TRAINING THAT AFTER V1 CALL YOU CONTINUE; HOWEVER; IN THIS SIT; THE ACFT DID NOT WANT TO LIFT OFF. THE DECISION TO ABORT THEREFORE MAY HAVE BEEN CALLED 1-2 SECONDS LATER. IN TRAINING; I HAVE EXPERIENCED A PITCH JAM IMMEDIATELY AFTER BEING AIRBORNE; BUT NEVER THE SIT WE EXPERIENCED. I WOULD LIKE TO POINT OUT THAT OUR WT AND BAL WAS CALCULATED CORRECTLY AND WE WERE LOADED FORWARD CTR OF GRAVITY BUT WITHIN NORMAL TKOF LIMITS.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.