AFTER EXTENSIVE DELAY (MECHANICAL PROBS); AN ACR FLC DEPARTED WITHOUT PERFORMING POST-MAINT WALK-AROUND. ACFT FAILED TO PRESSURIZE; DUE TO AN OPEN EQUIP BAY DOOR.
Synopsis
AFTER EXTENSIVE DELAY (MECHANICAL PROBS); AN ACR FLC DEPARTED WITHOUT PERFORMING POST-MAINT WALK-AROUND. ACFT FAILED TO PRESSURIZE; DUE TO AN OPEN EQUIP BAY DOOR.
Narrative
ON TKOF OUT OF MOBILE; AL; BOUND FOR CVG; THE ACFT WOULD NOT PRESSURIZE. WE HAD ONLY FLT; AND CABIN CREW; ON BOARD; THE FLT DIVERTED TO ATL WITH NO FURTHER PROBS. IT WAS LATER DETERMINED THAT THE E&E COMPARTMENT DOOR HAD NOT BEEN CLOSED CORRECTLY. THIS WAS AFTER LNDG ATL. ALSO; THE E&E DOOR WARNING SYS IN THE COCKPIT; WAS FOUND TO BE INOP. WE HAD NO ABNORMAL INDICATIONS; IN THE COCKPIT; OTHER THAN A LACK OF PRESSURIZATION. I COMPLETED A WALK- A-ROUND INSPECTION PRIOR TO PUSHBACK; BUT OBVIOUSLY DID NOT CATCH THE DOOR. IN THE AREA OF CONTRIBUTING FACTORS: EXTENSIVE MAINT HAD BEEN PERFORMED ON THE ACFT FOR SEVERAL HRS; PLUS 2 SEPARATE ENG RUNUPS PERFORMED BY FLC. NUMEROUS BAYS AND PANELS WERE OPENED AND REMOVED BY MAINT PERSONNEL. ON THE EXTERIOR INSPECTION I FOUND NICKS IN FAN BLADES FROM THE LAST ENG RUNUP. I DID A COMPLETE INSPECTION BUT CONCENTRATED ON ALL THE PANELS AND BAYS THAT HAD BEEN OPENED. ALSO WE WERE UNDER TIME PRESSURE TO GET THE ACFT TO CVG. MAINT BLENDED THE NICKS ON THE BLADES; AND WE WERE DISPATCHED. ALL THESE DISTRS PLUS THE WARNING SYS BEING INOP (UNKNOWN TO THE CREW) CAUSED THE PROB. SUPPLEMENTAL INFO FROM ACN 296861: THE CAPT DID THE LAST WALK AROUND AND ALL APPEARED TO BE OK. HOWEVER WE WERE BOTH IN THE COCKPIT REACCOMPLISHING A COMPLETE PREFLT (INTERIOR INSPECTION). WHILE THE MAINT MAN FINISHED UP HIS WORK OUTSIDE AND COMPLETED THE LOGBOOK.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.