PLT OF AN SMA SEL TURNED THE WRONG WAY AFTER TKOF. ON AN INST DEP.

Date: 1995-04 · Aircraft: Skylane 182/RG Turbo Skylane/RG · Phase: climb

Anomalies: aircraft-equipment-problem-less-severe|deviation-track-heading-all-types|deviation-discrepancy-procedural-clearance|other-unspecified

Synopsis

PLT OF AN SMA SEL TURNED THE WRONG WAY AFTER TKOF. ON AN INST DEP.

Narrative

THE TKOF ON AN IFR CLRNC WAS FROM RWY 29R TO JEFFCO ARPT. WITH THE DEP CLRNC TWR INSTRUCTED ME TO TURN R 'ALL THE WAY ROUND TO 150 DEGS' AFTER TKOF. SHORTLY AFTER LIFTOFF I DISCOVERED THAT MY FLAPS HAD FAILED TO RETRACT COMPLETELY. THEY REMAINED IN TRAIL ABOUT 3 DEGS. WHILE CHKING FOR THE CAUSE; I MONITORED 2 ACFT TO MY L OPERATING VFR OFF RWY 29L. WHEN I OBSERVED THEM TURNING L AWAY FROM ME I GAVE MY FULL ATTN TO THE FLAP PROB; RESOLVED IT; THEN BEGAN THE TURN TO 150 DEGS. UNFORTUNATELY; WHEN I LOOKED AT MY DIRECTIONAL GYROSCOPE TO ORIENT MYSELF BEFORE COMMENCING THE TURN I NOTED THAT 150 DEGS IN THE L REAR QUADRANT OF THE INST. THIS WOULD NORMALLY CALL FOR A L TURN; SO I BANKED L WHILE CONTINUING TO OBSERVE THE VFR ACFT; ALSO IN L TURNS. AFTER ABOUT 20 DEGS OF TURNING THE TWR CTLR ASKED WHICH DIRECTION I WAS TURNING. I IMMEDIATELY RECALLED THAT THE INSTRUCTIONS HAD BEEN TO TURN R TO 150 DEGS AND REVERSED THE TURN. MY ERROR WAS IN NOT CONSIDERING THE SIT BEFORE DEP. SINCE I WAS SEBOUND AND MY TKOF WAS ON RWY 29R WITH SIMULTANEOUS VFR OPS BEING CONDUCTED FROM RWY 29L; I SHOULD HAVE REALIZED THAT SOME SPECIAL PROC WOULD BE REQUIRED TO AVOID CONFLICTS. THAT WOULD HAVE OBVIOUSLY BEEN A CLB STRAIGHT AHEAD TO WELL ABOVE PATTERN ALT OR A TURN THE LONG WAY AROUND TO THE SE. WHICH DEMONSTRATES ONCE MORE THAT IF WE PAY ATTN WE LEARN SOMETHING NEW EVERYDAY. I MUST RESOLVE TO DO THAT IN THE FUTURE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: RPTR STATED THAT HE HAD REACHED APPROX 600 FT ABOVE THE GND PRIOR TO TURNING THE WRONG WAY AND WAS OPERATING HIS CESSNA 182. HE FURTHER STATED THAT THE MOMENTARY LACK OF COMPLETE FLAP RETRACTION WAS FOUND TO BE CAUSED BY THE FLAP MOTOR WHICH WAS REPLACED.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.