CHARTER PLT OF AN SMA RELIED ON FUEL QUANTITY INFO FROM COMPANY OPS INSTEAD OF PHYSICALLY VERIFYING THE AMOUNT OF FUEL ON BOARD. THE OUTCOME OF THE FLT INVOLVED A FORCED LNDG DUE TO FUEL EXHAUSTION.
Synopsis
CHARTER PLT OF AN SMA RELIED ON FUEL QUANTITY INFO FROM COMPANY OPS INSTEAD OF PHYSICALLY VERIFYING THE AMOUNT OF FUEL ON BOARD. THE OUTCOME OF THE FLT INVOLVED A FORCED LNDG DUE TO FUEL EXHAUSTION.
Narrative
I WAS ON A RETURN LEG OF A FLT FROM GAINSVILLE; FL; TO ST PETERSBURG; FL. THE WX THAT DAY WAS LOW OVCST AND IFR. AS I WAS NEARING BKV; ENRTE TO SPG MY ENG STARTED TO RUN ROUGH TO THE POINT WHERE IT WOULDN'T RUN ANYMORE. SUSPECTING WATER FROM THE HVY RAIN WHICH I WAS FLYING IN; I SWITCHED FUEL TANKS. THE ENG RAN NORMAL AFTER THAT POINT FOR ABOUT 60 SECONDS; AFTER WHICH IT HAPPENED AGAIN. NOW I HAD ABSOLUTELY NO PWR. KNOWING OF MY POS RELATIVE TO BKV; I ASKED TPA APCH FOR HELP FINDING THE ARPT. I DECLARED AN EMER TO RECEIVE THE CTLR'S FULL ATTN; AND AFTER HE TOLD ME I WAS ONLY 4 MI FROM BKV ARPT I FELT RELIEVED. I CONTINUED TO GLIDE DOWN; FOLLOWING HIS INSTRUCTIONS; TOTALLY IN IMC. I BROKE OUT OF THE WX ABOUT 300-500 FT AGL OVER BKV IN A STEEP SPIRAL AND MADE A VERY SAFE LNDG. AFTER I EXITED THE AIRPLANE TO CHK FOR FUEL CONTAMINATION I THEN REALIZED WHAT HAD HAPPENED. THAT MORNING I WAS MISINFORMED OF MY FUEL AMOUNT FROM MY OPS. THINKING THE ENTIRE DAY THAT I HAD 30 GALS MORE THAN I ACTUALLY HAD. I RAN OUT OF FUEL OVER BKV WHICH WAS A RESULT OF AN IFR DEP WITHOUT THE REQUIRED FUEL PLUS 45 MINS RESERVE.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.