NIGHT OP ACR FREIGHTER FLC FAILS TO HAVE THE CAPT'S PITOT HEATER CHKED PRIOR TO DEP AS PER THE PROVISIONS OF THE MEL REQUIREMENTS ON DEP FROM THEIR SECOND ARPT. FLC DISTR ACFT EQUIP PROB.

Date: 1996-11 · Aircraft: Commercial Fixed Wing · Phase: ground

Anomalies: aircraft-equipment-problem-less-severe|deviation-discrepancy-procedural-far|deviation-discrepancy-procedural-other-unknown|deviation-discrepancy-procedural-published-material-policy|other-unspecified

Synopsis

NIGHT OP ACR FREIGHTER FLC FAILS TO HAVE THE CAPT'S PITOT HEATER CHKED PRIOR TO DEP AS PER THE PROVISIONS OF THE MEL REQUIREMENTS ON DEP FROM THEIR SECOND ARPT. FLC DISTR ACFT EQUIP PROB.

Narrative

THE CAPT PITOT HEAT AMMETER WAS DEFERRED DUE TO LOW PWR INDICATION. THE DEFERRAL (MEL ITEM) REQUIRED AN INSPECTION PRIOR TO EACH FLT. THE CAPT PITOT HEAT WAS INSPECTED BY MAINT AT THE ORIGINATING ARPT (PHL) AND FOUND TO BE OPERATING. THE AMP INDICATION ON THE DEFERRED METER WAS NORMAL ALSO. THE CAPT PITOT HEAT INSPECTION AT THE ENRTE STOP (DTW) WAS OVERLOOKED AND DID NOT OCCUR. I DO NOT KNOW WHY THE INSPECTION WAS MISSED BY MAINT; BUT SOME OF THE FACTORS THAT MAY HAVE LED TO THE INSPECTION BEING OVERLOOKED BY THE FLC ARE: 1) THE AMMETER WAS OPERATING NORMALLY. 2) THE DEFERRED STICKER ON THE AMMETER WAS A NORMAL WHITE STICKER. AN ITEM REQUIRING A REPETITIVE INSPECTION IS SUPPOSED TO HAVE AN ORANGE STICKER TO CALL EVERYONE'S ATTN TO THE REPETITIVE INSPECTION. 3) THE FLT LANDED AT DTW WITH A REAL MECHANICAL PROB. THERE WAS A PNEUMATIC OVERPRESSURE INDICATION ON THE #3 ENG. THIS WAS WRITTEN UP BY THE FLC AND DEFERRED BY MAINT AT DTW. THE PROCESS TOOK ABOUT 45 MINS AND REQUIRED A PHONE CALL TO THE DISPATCHER TO DETERMINE IF IT WAS LEGAL TO CONTINUE TO LAN DUE TO POSSIBLE ICING CONDITIONS. THE REPETITIVE INSPECTION WAS MISSED. IN MY OPINION; THE SAFETY OF THE FLT WAS NOT AFFECTED BECAUSE THE AMMETER AND PITOT HEAT WERE WORKING NORMALLY AND ICING CONDITIONS DID NOT EXIST. SUPPLEMENTAL INFO FROM ACN 352629: FATIGUE: THIS WAS OUR THIRD FLT OF THE NIGHT WHICH HAD STARTED AT AB00 PM. IT WAS NOW AK00 AM. WE HAD DEPARTED PHL LATE AND DTW GND PERSONNEL WERE EAGER TO BLOCK US OUT. I BELIEVE THE FAA SHOULD SHORTEN CONSIDERABLY THE ALLOWABLE DUTY TIMES DURING THE NIGHT DUE TO CIRCADIAN RHYTHM INDUCED FATIGUE.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.