ACR MLG ELECTED TO START BOTH ENGS ON PUSHBACK ACCOUNT SHORT TAXI. CAPT TURNED OFF THE IGNITOR AFTER FIRST ENG STARTED. #2 DID NOT LIGHT OFF AND THE ENG WAS MOTORED TO CLR FUEL BUT THE FO FAILED TO TURN OFF THE FUEL. ON SECOND ATTEMPT ENG STARTED AND THEN EXCEEDED START LIMITS OF 475 DEGS AND TOPPED OUT AT 620 DEGS. RETURNED TO THE GATE AND FLT CANCELED. OVERTEMP RESULTED IN ENG CHANGE.
Synopsis
ACR MLG ELECTED TO START BOTH ENGS ON PUSHBACK ACCOUNT SHORT TAXI. CAPT TURNED OFF THE IGNITOR AFTER FIRST ENG STARTED. #2 DID NOT LIGHT OFF AND THE ENG WAS MOTORED TO CLR FUEL BUT THE FO FAILED TO TURN OFF THE FUEL. ON SECOND ATTEMPT ENG STARTED AND THEN EXCEEDED START LIMITS OF 475 DEGS AND TOPPED OUT AT 620 DEGS. RETURNED TO THE GATE AND FLT CANCELED. OVERTEMP RESULTED IN ENG CHANGE.
Narrative
NORMAL PUSHBACK AT SDF. SHORT TAXI TO RWY 17; SO I CALLED FOR BOTH ENGS TO BE STARTED. I OPERATED THE FUEL SWITCH FOR #1; AS I ALWAYS DO; WHILE THE FO OPERATED THE FUEL LEVER AND MONITORED THE START. THE START WAS NORMAL. I APPARENTLY TURNED OFF THE IGNITION AFTER THE START; AS IS MY HABIT. WHEN THE FO WENT TO START #2 (WHILE I SALUTED OFF THE GND CREW); HE DID NOT NOTICE THE IGNITION SWITCH OFF. NATURALLY THE ENG FAILED TO LIGHT OFF. THE FO ANNOUNCED THIS; AND I ASSUMED HE HAD SHUT OFF THE FUEL. NORMALLY; I WOULD HAVE SAID SOMETHING ABOUT MOTORING AT THIS POINT; BUT WHEN I LOOKED UP FROM TAXIING IT APPEARED HE HAD JUST FINISHED MOTORING IT. WE READ THE TAXI LIST WHILE THE ENG WOUND DOWN. I WAS TAXIING SLOWLY BECAUSE IT WAS A SHORT TAXI; I HADN'T ALERTED THE FLT ATTENDANTS ABOUT IT; AND I DIDN'T WANT THE CREW RUSHED. AT THIS POINT; THE FO REACHED UP AND BEGAN RESTARTING #2. I GLANCED AT THE EGT TO MAKE SURE IT DIDN'T SHOW ANY RESIDUAL FUEL TORCHING. INITIALLY IT WAS FINE; THEN SUDDENLY WENT UP RAPIDLY. I ANNOUNCED THIS FACT; BUT IT KEPT ON GOING TO ABOUT 620 DEGS C (MAX IS 475 DEGS C). AT THIS POINT WE BOTH REALIZED THAT THE FUEL LEVER FROM #2 WAS STILL ON FROM THE ORIGINAL START. WE RETURNED TO THE GATE; THE FLT WAS CANCELED; AND THE ENG CHANGED. THIS HAS BEEN A VERY DISTURBING EXPERIENCE FOR BOTH THE FO AND MYSELF. THIS WAS NOT TYPICAL OF THE FO'S NORMAL PERFORMANCE. I AM FURTHER FRUSTRATED THAT I DID NOT STOP THE TAXI COMPLETELY AND ENSURE THE ABORTED START PROC WAS IMPLEMENTED COMPLETELY AND PROPERLY. WHILE I HAVE DEALT WITH ABORTED STARTS NUMEROUS TIMES IN MY CAREER; I SHOULD REALIZE THAT MANY OF OUR FO'S HAVE NOT.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.