A B777; IMMEDIATELY AFTER TKOF AT 200 FT; DECLARED AN EMER AND DIVERTED DUE TO SMOKE IN THE COCKPIT CAUSED BY A FAILED #1 ENG AND ENG OIL FIRE.

Date: 1998-07 · Aircraft: B777 Undifferentiated or Other Model

Anomalies: aircraft-equipment-problem-critical|other-unspecified

Synopsis

A B777; IMMEDIATELY AFTER TKOF AT 200 FT; DECLARED AN EMER AND DIVERTED DUE TO SMOKE IN THE COCKPIT CAUSED BY A FAILED #1 ENG AND ENG OIL FIRE.

Narrative

IMMEDIATELY AFTER TKOF FROM RWY 27L; THE COCKPIT BEGAN TO FILL WITH SMOKE. CREW DONNED OXYGEN MASKS. I DECLARED AN EMER WITH HEATHROW TWR. A FEW SECONDS LATER THE PURSER RPTED THE CABIN WAS FILLING WITH SMOKE. SMOKE WAS DENSE AND INCREASING RAPIDLY. I TURNED OFF THE RWY CTRLINE TO POS THE ACFT FOR A COURSE REVERSAL AND IMMEDIATE DOWNWIND LNDG IF IT BECAME NECESSARY. UPON AUTOTHROTTLE THRUST REDUCTION; THE L ENG SEIZED. WE SECURED THE ENG. THE SMOKE BEGAN TO DISSIPATE AND WE FLEW A VISUAL L-HAND PATTERN TO A SINGLE ENG LNDG ON RWY 27L AT LHR. OVERWT LNDG; AT APPROX 547500 LBS. TOUCHDOWN SMOOTH; ROLLOUT NORMAL. CLRED RWY; HAD CFR INSPECT ACFT. TAXIED TO GATE WITH FIRE ESCORT. DEPLANED PAX AT GATE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE FIRST HINT OF TROUBLE WAS SMOKE IN THE COCKPIT AND IT WAS NOT JUST THE TYPICAL SMELL AND ACRID ODOR OF OVERHEATED DUCTING; BUT SMOKE FROM THE BURNING ENG OIL. THE RPTR SAID AFTER SHUTTING THE ENG DOWN THE SMOKE DISSIPATED. THE RPTR SAID THE L ENG INDICATIONS WERE INOP AND WHEN ON THE GND IT WAS FOUND AN EXTERNAL OIL FIRE HAD BURNED THROUGH THE ALUMINUM ELECTRICAL CONDUIT DAMAGING THE WIRING. THE LCL MAINT PEOPLE BELIEVED THE #2 BEARING OIL SEAL FAILED CAUSING THE LOSS OF OIL PRESSURE AND QUANTITY BUT DID NOT EXPLAIN THE BURN THROUGH THAT CAUSED THE EXTERNAL OIL FIRE. THE RPTR STATED THE ENG WAS IMPOUNDED BY THE BRITISH CIVIL AERO BOARD AND THE NTSB AND SENT TO THE MANUFACTURER FOR ENG TEARDOWN AND INVESTIGATION. THE RPTR SAID LCL MAINT RPTED THE ENG WAS NOT SEIZED BUT THE RPTR WITNESSED A MECH ATTEMPTING TO TURN THE FAN AND COULD NOT MOVE IT. THE RPTR STATED THAT AFTER A REVIEW OF THE EVENTS IN THE COCKPIT DURING THE EMER SOME PROCS NEED TO BE REVISED SUCH AS GIVING THE RELIEF PLT ADDITIONAL DUTIES TO PERFORM. CALLBACK CONVERSATION WITH RPTR ACN 409690 REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ACFT TOOK OFF AT MAX GROSS WT AND AT 200 FT DISCOVERED SMOKE ROLLING OUT FROM UNDER THE RPTR'S INST PANEL AND THEN NOTICED A LOSS OF THRUST. THE RPTR SAID THE ACFT WAS CLBED AT 400 FPM AND AT 230 KTS. CALLBACK CONVERSATION WITH RPTR ACN 409689 REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CAUSE OF THE ENG FAILURE IS BELIEVED TO BE THE #2 BEARING OIL SEAL FAILURE AND THIS ENG WAS THE LAST ENG IN THE FLEET THAT NEEDED TO BE MODIFIED WITH THE NEW BEARING SEAL. THE RPTR SAID THE TOTAL FLYING TIME WAS A TOTAL OF 12 MINS. THE RPTR STATED THE ENG WAS IMPOUNDED FOR INVESTIGATION AND TEARDOWN BY THE MANUFACTURER.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.