A B737-200 WAS DISPATCHED IN NON COMPLIANCE WITH A GND SPOILER REPAIR MADE IN CONFLICT WITH THE MAINT MANUAL AND STRUCTURAL REPAIR MANUAL.
Synopsis
A B737-200 WAS DISPATCHED IN NON COMPLIANCE WITH A GND SPOILER REPAIR MADE IN CONFLICT WITH THE MAINT MANUAL AND STRUCTURAL REPAIR MANUAL.
Narrative
MECH WAS INSTRUCTED TO COMPLETELY REPLACE TOP; BOTTOM SKINS AND HONEYCOMB CORE ON GND SPOILER. B737-200 PART NUMBER 65-46452 IS AN ALUMINUM HONEYCOMB SANDWICH -- BUILT AND BONDED TOGETHER USING MOLDS AND AUTOCLAVE. THIS SPOILER WAS REBUILT TO A MUCH LOWER STRENGTH THAN ORIGINAL; USING ONLY VACUUM BAG METHODS AND NO MOLDS. AFTER 3 ATTEMPTS TO PASS INSPECTION (BOND VOIDS WERE FOUND); IT IS NOW IN THE PARTS SYS. THE GREATER PROB IS THAT THIS 'NEW' PROCESS HAS BEEN ADOPTED FOR OTHER DAMAGED ALUMINUM FLT CTLS. HAVE TRIED TO CORRECT PROB WITH INTERNAL HOTLINE CALL WITHOUT RESOLUTION. HAVE SUGGESTED THAT THE ON-SITE BOEING REPRESENTATIVE BE ASKED IF REBUILDING FLT CTLS USING ONLY VACUUM BAG METHODS IS ACCEPTABLE -- SAYS HE IS NOT AN ENFORCEMENT AGENCY. THERE IS A MEMO FROM ENGINEERING WHICH CHANGES THE READING OF SRM INSTRUCTIONS TO ALLOW VACUUM BAG ONLY ON CURVED SURFACES. THIS SAVES SEVERAL MILLION DOLLARS IN MOLDS AND AUTOCLAVE EQUIP; AND GIVES US A LEG UP ON THE COMPETITION (WHO USE AUTOCLAVES). CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE PROC THAT ENGINEERING HAS ALLOWED FOR FLAT COMPOSITE SURFACES WHICH IS IN CONFLICT WITH THE STRUCTURAL REPAIR MANUAL HAS NOW BEEN APPROVED BY THE COMPANY ENGINEERING TO USE ON CURVED SURFACES. THE RPTR SAID THIS PROB HAS BEEN ONGOING FOR A LONG TIME AND HAS RESULTED IN FLT CTL SURFACES FROM ALL ACFT OWNED BY THE COMPANY CYCLING THROUGH THE SHOP WITH POOR SVC TIME. THE RPTR SAID WITHOUT THE PROPER TOOLING A GOOD REPAIR CANNOT BE ACCOMPLISHED.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.