AN MD80 ON TKOF AT ROTATION WITH HVY XWIND GUSTS EXPERIENCED BOTH ENGS COMPRESSOR STALL; LATER DETERMINED TO BE CAUSED BY COMPRESSOR DETERIORATION.

Date: 2000-01 · Aircraft: MD-80 Series (DC-9-80) Undifferentiated or Other Model · Phase: takeoff

Anomalies: aircraft-equipment-problem-critical|other-engine-stall

Synopsis

AN MD80 ON TKOF AT ROTATION WITH HVY XWIND GUSTS EXPERIENCED BOTH ENGS COMPRESSOR STALL; LATER DETERMINED TO BE CAUSED BY COMPRESSOR DETERIORATION.

Narrative

RIGHT AT ROTATION ON TKOF; WE NOTICED A SLIGHT HESITATION OF THE ACFT AND A BLINK OF THE MASTER CAUTION LIGHT. OUR INITIAL THOUGHT WAS THAT THE ACFT HAD BEEN BUFFETED BY THE STRONG GUSTING WINDS THAT WERE PRESENT DURING TKOF. TKOF AND CLBOUT WERE UNEVENTFUL. SEATBELT SIGN WAS TURNED OFF AND THE FLT ATTENDANT FROM THE REAR CAME FORWARD AND ASKED IF THAT WAS A COMPRESSOR STALL ON TKOF. SHE SAID IT WAS A LOUD (BUT NOT EXTREMELY LOUD OR EXPLOSIVE) NOISE FROM BOTH ENGS DURING ROTATION. THE ENG'S INSTS WERE CHKED AGAIN AND WERE NORMAL. THE ENGS RAN SMOOTHLY DURING ACCELERATION AND DECELERATION AND AT STEADY STATE WITH NO ABNORMAL ENG INST INDICATIONS. NOT HEARING THE NOISE FROM THE COCKPIT WE SURMISED WE MAY HAVE HAD A LIGHT TO MODERATE COMPRESSOR STALL ON BOTH ENGS. SINCE THE FLT HANDBOOK CLASSIFIED A COMPRESSOR STALL AS AN ADDITIONAL PROC WHICH IS DEFINED AS A MINOR PROB AND THAT THE ENGS WERE OPERATING NORMALLY; WE CONTINUED TO ST LOUIS AND LANDED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ENG'S MOMENTARY STALL WAS NOT NOTICEABLE IN THE COCKPIT AND THE APPARENT BUFFET WAS ATTRIBUTED TO A XWIND GUST. THE RPTR SAID THE FLT ATTENDANT SITTING ON THE R AFT SEAT RELATED THE STALL WAS FROM THE L ENG AND THE FLT ATTENDANT SITTING ON THE L AFT SEAT STATED THE STALL WAS FROM THE R ENG. THE RPTR SAID THE MD80 ENGS COULD POSSIBLY HAVE BEEN AFFECTED BY THE XWIND GUSTS AND THE COMPRESSOR CONDITION THAT WAS DISCOVERED ON TRIP TERMINATION. THE RPTR STATED AT TRIP TERMINATION THE ACFT WAS REMOVED FROM SVC AND THE ENGS WERE INSPECTED REVEALING COMPRESSOR DAMAGE. THE RPTR SAID MAINT DETERMINED THE DAMAGE WAS CAUSED BY INGESTION OF PEA GRAVEL ON A PREVIOUS FLT.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.