AN MD80 ON 3 MI FINAL AT 1000 FT HAD NOSE LNDG GEAR FAIL TO EXTEND. EXTENDED ON GAR BUT INCURRED LOSS OF R HYD SYS. CAUSE UNKNOWN.

Date: 2001-08 · Aircraft: MD-80 Series (DC-9-80) Undifferentiated or Other Model

Anomalies: aircraft-equipment-problem-critical|other-loss-of-right-hydraulic

Synopsis

AN MD80 ON 3 MI FINAL AT 1000 FT HAD NOSE LNDG GEAR FAIL TO EXTEND. EXTENDED ON GAR BUT INCURRED LOSS OF R HYD SYS. CAUSE UNKNOWN.

Narrative

ON FINAL FOR RWY 4R AT ORD; FO WAS FLYING; AND ASKED FOR GEAR DOWN. I LOWERED THE HANDLE; BUT THE GEAR DID NOT COME DOWN. I CHKED HYD SWITCHES IN THE ON HIGH/HIGH/ON. AFTER A FEW SECONDS; THE MAIN GEAR BOTH CAME DOWN 'GREEN' BUT THE NOSE GEAR STILL INDICATED UNSAFE. R HYD QUANTITY WAS NEAR ZERO; BUT PRESSURE WAS NEAR NORMAL THOUGH IT WAS UNSTEADY. WITH NO SAFE NOSE GEAR INDICATION WE WENT AROUND. DURING THE GAR; THE NOSE GEAR CAME DOWN AND INDICATED SAFE. WE LEFT THE GEAR DOWN. THE R HYD QUANTITY WAS STILL NEAR ZERO; BUT THE PRESSURE WAS NOW STABLE AND NORMAL. THE L SYS OPERATED NORMALLY THROUGHOUT. WE LANDED NORMALLY. SINCE OUR GATE WAS OCCUPIED; GND SENT US TO RWY 32R PAD. AS SOON AS I PARKED THE BRAKES; AN EMPLOYEE IN THE BACK SAID HE HEARD A GRINDING SOUND NEAR THE R ENG. I DECIDED TO TURN OFF THE HYDS TO THE R SYS. I THEN REQUESTED THAT MAINT COME OUT AND PIN THE GEAR WITH NO PRESSURE ON THE GEAR. WE THEN TAXIED IN NORMALLY. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE EXACT COMPONENT THAT CAUSED THE LOSS OF FLUID AND PRESSURE IS UNKNOWN. THE RPTR SAID MAINT HAS NOT ADVISED THE CREW OF THE MAINT ACTION TAKEN.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.