TWIN TURBOPROP PLT STRUCK ICE DURING TKOF AT A RWY INTXN CAUSING DAMAGE TO THE NOSE GEAR ACTUATOR ASSEMBLY RESULTING IN THE NOSE GEAR COLLAPSING DURING THE SUBSEQUENT EMER LNDG.
Synopsis
TWIN TURBOPROP PLT STRUCK ICE DURING TKOF AT A RWY INTXN CAUSING DAMAGE TO THE NOSE GEAR ACTUATOR ASSEMBLY RESULTING IN THE NOSE GEAR COLLAPSING DURING THE SUBSEQUENT EMER LNDG.
Narrative
ON JAN/MON/02 AT ABOUT XA00; I WAS MAKING A TKOF ON RWY 23 AT THE YNG ARPT. ALTHOUGH THERE HAD BEEN SNOW THE NIGHT BEFORE; AND THIS RWY WAS CLOSED WHEN I ARRIVED AT ABOUT XB15; THE SNOW HAD BEEN REMOVED AND THE RWY APPEARED TO BE BARE AND WET WHEN I TAXIED ONTO IT FOR TKOF. JUST E OF THE INTXN OF THIS RWY AND THE MAIN INST RWY 14/32; AT A SPD OF ABOUT 80 KTS; I ENCOUNTERED AN AREA OF SLUSH WHICH DUE TO ITS GRAY COLOR AND THE CONCRETE COLOR OF THE RWY WAS ALMOST INVISIBLE. WHEN I ATTEMPTED TO RAISE THE LNDG GEAR AFTER AIRBORNE; THERE WAS A FAILURE OF THE NOSE GEAR ACTUATOR. I WAS UNABLE TO GET A DOWN AND LOCKED INDICATION ON THE NOSE GEAR. I DID 2 FLY-BY-THE-TWR PASSES AND THEY TOLD ME THAT ALL LNDG GEAR LOOKED NORMAL. I DECLARED AN EMER AND ON LNDG; THE NOSE GEAR COLLAPSED. I WENT BACK TO THE AREA WHERE I ENCOUNTERED THE SLUSH AND FOUND IT TO BE RIGHT ON THE RWY CTRLINE; ABOUT 8-10 FT IN DIAMETER; WITH A DEPTH OF 2-3 INCHES. BASED UPON THE INITIAL FINDINGS OF THE MAINT DEPT; THE SLUSH ENCOUNTER DAMAGED ONE OR BOTH OF THE GEAR DOORS SUCH THAT THE LNDG GEAR TRIED TO RETRACT THROUGH IT; AND BROKE THE ACTUATOR. THE SLUSH PILE ON THIS RWY IN THIS SPOT WAS LIKELY THE RESULT OF PLOWING OPS ON THE MAIN RWY. THIS RWY AND THE INTXN SHOULD HAVE BEEN INSPECTED AFTER THE PLOWING OP WAS FINISHED ON THE OTHER RWY. RWY 23 SHOULD HAVE BEEN CLOSED UNTIL THE SLUSH AREA WAS REMOVED.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.