C172 INSTRUCTOR AND STUDENT HAD INDICATIONS OF ALTERNATOR FAILURE. THE ACFT OP WAS CONTINUED UNTIL THE BATTERY DIED.
Synopsis
C172 INSTRUCTOR AND STUDENT HAD INDICATIONS OF ALTERNATOR FAILURE. THE ACFT OP WAS CONTINUED UNTIL THE BATTERY DIED.
Narrative
AN INFLT ELECTRICAL FAILURE OCCURRED FOR THE ELECTRICAL CHARGING SYS OF THE C172. THE AIRPLANE JUST HAD AN INSTALLATION OF A GARMIN 430 MOVING MAP; DAUTRON DIGITAL CLOCK; AND GARMIN INDICATOR. ACFT CHKED OUT NORMALLY WHEN PREFLTED AND RUN-UP AMMETER INDICATED NORMALLY WHEN FIELD SWITCH TURNED OFF DURING GND CHKS. BATTERY HAD LESS THAN 10 HRS OF OP ON IT SINCE NEW. NOT MUCH DISCHARGE OCCURRED DURING THE 5-6 CIRCUITS OF FIELD OFF. IN CRUISE FLT; DISCHARGE LIGHT WAS DIMLY LIT. ALTERNATOR FIELD ROCKER SWITCH WAS CYCLED 3 TIMES. SYS SEEMED TO BE BEHAVING NORMALLY; BUT ELECTRICAL EQUIP THAT WAS NON ESSENTIAL WAS TURNED OFF. AFTER 1 HR AND 10 MINS OF FLT; RADIO RECEPTION AND XMISSION CAPABILITY WAS LOST. SQUAWKED 7600 INTERMITTENTLY. WHEN GARMIN GNS LBO WENT OFF LINE; COM RECEPTION WAS RESTORED LONG ENOUGH TO GET VECTORS FROM GREER APCH TO A LOC RWY 1 AT GMV. NAV RECEPTION OF #2 NAV/COM WAS LOST WHILE DSNDING THROUGH CLOUDS. HANDHELD GARMIN III PLT WAS USED FOR EMER COURSE GUIDANCE TO LOC MINIMUMS AT GMV. A NORMAL LNDG AT GMV WAS THEN EXECUTED ONCE VISUAL.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.