BONANZA PLT HAS ENG MALFUNCTION DURING APCH TO ILL AND ELECTS TO DO AN OFF FIELD LNDG.
Synopsis
BONANZA PLT HAS ENG MALFUNCTION DURING APCH TO ILL AND ELECTS TO DO AN OFF FIELD LNDG.
Narrative
DEPARTED ZZZ1 TO ZZZ2. PRE-LNDG CHKLIST HAD FUEL ON L MAIN; MIXTURE RICH AND ENTERED DOWNWIND AT 45 DEGS FOR RWY 28; GEAR DOWN; 15 DEG MANIFOLD PRESSURE. BEGAN L BANK TURN TO BASE. ENG LOST PWR AS I GAVE MORE THROTTLE AND NO RESPONSE. A QUICK CHK OF FUEL SELECTOR VERIFIED L MAIN AND NO ENG RESPONSE. ALT WAS APPROX 500 FT AGL. AT THE END OF RWY 10 IS A DRAINAGE DITCH. I KNEW I WAS NOT GOING TO MAKE THE RWY AND HAD PWR LINES AND TREES TO CONTEND WITH. I FEATHERED THE PROP AND RETRACTED THE FLAPS. CLRED THE TREES AND LANDED IN A BEAN FIELD APPROX 1/8 MI FROM THE ARPT. NO DAMAGE TO THE ACFT OR MYSELF. UPON INSPECTION; FUEL SELECTOR WAS ON L MAIN AND VISUAL INSPECTION SHOWED TANK TO BE 3/4 FULL. ACFT R FUEL VENT WAS CLR. THE L VENT WAS SLIGHTLY BLOCKED AND WAS BLOWN OUT. ACFT WAS TOPPED OFF AND TOOK 47 GALS. 63 GALS USABLE MEANT 16 GALS WERE IN THE L MAIN. TEMP AT THE TIME WAS UPPER 30 DEGS. THE MECH HAD NO SOLID EXPLANATION. ICE MIGHT HAVE BEEN A POSSIBILITY OR THE PARTIALLY BLOCKED L VENT. THE ACFT WAS CHKED OUT; MAGNETOS; VENTS; RUN-UP; ETC; AND FLOWN HOME THE SAME DAY. THE ACFT HAD A CHK VALVE REPLACED DUE TO FUEL LEAKAGE 6 MONTHS PRIOR. IT HAD NOT BEEN A PROB SINCE THAT TIME. WE ARE GONG TO CONTACT THE BONANZA ORGANIZATION FOR THEIR THOUGHTS ON THIS SIT.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.