A B767-300 IN CRUISE AT FL390 DECLARED AN EMER AND DIVERTED DUE TO R ENG FLAMEOUT. CAUSED BY BROKEN FUEL FITTING ON ENG.
Synopsis
A B767-300 IN CRUISE AT FL390 DECLARED AN EMER AND DIVERTED DUE TO R ENG FLAMEOUT. CAUSED BY BROKEN FUEL FITTING ON ENG.
Narrative
ABOUT 2 HRS AFTER TAKING OFF FROM ZZZ WE HAD EICAS STATUS MESSAGES OF: R ENG CONT; R ENG EEC C1; R ENG A/O VALVE; R IDG VALVE. WE CONTACTED MAINT AND BRIEFED HIM ON THE STATUS MESSAGES AND ENG PARAMETERS. SHORTLY AFTER THAT WE HAD AN INDICATION OF A FUEL IMBAL BY THE FUEL CONFIGN LIGHT AND EICAS MESSAGE. WE BALANCED THE FUEL ACCORDING TO THE INDICATION OF R TANK LOW. LATER WE RECOGNIZED AN INCREASING IMBAL BTWN THE TOTALIZER AND CALCULATED FUEL ON THE PROGRESS PAGE 2. WE THEN CONTACTED MAINT TO DISCUSS THE DISCREPANCY. WE DETERMINED THAT THIS WAS A GAUGE PROB AND THAT WE SHOULD NOT CONTINUE TO ATTEMPT TO BAL FUEL ACCORDING TO THE INDICATIONS. AFTER SOME TIME WE BECAME MORE CONCERNED WITH THE FUEL IMBAL AND TRIM INDICATIONS OF THE AIRPLANE. WE ATTEMPTED TO RETRIM THE AIRPLANE AND THEN REALIZED THAT THE R FUEL QUANTITY GAUGE WAS DECREASING MORE RAPIDLY. WE RECONTACTED MAINT AND WE AGREED TO PERFORM THE FUEL LEAK CHKLIST. WE THEN SENT A FLT ATTENDANT TO VISUALLY CHK ENGS AND FUEL FOR A LEAK. DURING THIS PROCESS; THE FUEL INDICATOR WAS DECREASING MORE RAPIDLY AND THE R ENG FLAMED OUT SHORTLY THEREAFTER. UPON ENG FLAMEOUT I DECLARED AN EMER WITH ATC AND ASKED FOR THE DRIFTDOWN CHKLIST. ONCE DSNDING AND THE CHKLIST COMPLETED WE INDICATED THAT WE WOULD GO TO ZZZ2 WITH CTR. I THEN ASKED FOR THE INFLT ENG FAILURE AND FLAMEOUT CHKLIST. WE WERE IN A CONSTANT DSCNT WITH CTR AS WE RAN THE CHKLIST TO THEIR COMPLETION. I ADVISED THE FIRST FLT ATTENDANT OF A CABIN ADVISORY FOR THE ENG FAILURE AND OR INTENTION OF LNDG IN ZZZ2. I SENT AN ACARS MESSAGE TO DISPATCH OF OUR DIVERSION. HE ACKNOWLEDGED OK. I THEN EXPLAINED TO THE PAX THAT WE WOULD LAND IN ZZZ2 DUE TO ENG FLAMEOUT AND THAT IT WOULD BE AN UNEVENTFUL LNDG. WE LANDED 20 DEGS FLAPS ON RWY 16R USING AUTOBRAKES 2 AND L REVERSER. THE FIRE TRUCKS FOLLOWED US TO A REMOTE PARKING SPOT AND WE CHKED FOR A FUEL LEAK. NONE WAS OBSERVED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ENG WAS A PRATT & WHITNEY JT9D-7R4 ENG AND HAD ONLY 35 HRS OF TIME IN SVC AND THE CAUSE OF THE FUEL LEAKAGE AND FLAMEOUT WAS A BROKEN FUEL LINE FITTING. THE RPTR SAID THE EXACT FITTING AND LOCATION OF THE FITTING ON THE ENG IS UNKNOWN AS MAINT HAS NOT RPTED ANY FINDINGS TO THE CREW.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.