A LEAR 25D AT FL390 HAD VIBRATION IN AIRFRAME AND LOUD BANG FROM THE L ENG; WHICH FLAMED OUT. THEY ATTEMPTED RELIGHT AT FL250 NO HELP. DECLARED EMER AND DIVERTED. THIS SAME ENG HAD FLAMEOUT EARLIER AND THE SAME FLT WAS ABLE TO RESTART SIX DAYS PRIOR TO THIS EVENT.
Synopsis
A LEAR 25D AT FL390 HAD VIBRATION IN AIRFRAME AND LOUD BANG FROM THE L ENG; WHICH FLAMED OUT. THEY ATTEMPTED RELIGHT AT FL250 NO HELP. DECLARED EMER AND DIVERTED. THIS SAME ENG HAD FLAMEOUT EARLIER AND THE SAME FLT WAS ABLE TO RESTART SIX DAYS PRIOR TO THIS EVENT.
Narrative
ACFT HAD LEVELED AT FL430 FOR APPROX 5 MINUTES. AUTOPLT ENGAGED WHEN THE CREW HEARD A LOUD NOISE FROM THE ACFT. I NOTICED THE L ENG RPM GAUGE DROP TO 30% AND THE ACFT EXHIBITED A YAWING EFFECT. I REALIZED AT THIS POINT THE L ENG HAD FAILED. I DISENGAGED THE AUTOPLT AND TOOK CTL OF THE ACFT. I INSTRUCTED THE FO TO ASK ATC FOR A LOWER ALT; WHICH WAS GRANTED IMMEDIATELY. WE DSNDED TO FL250 AND REQUESTED A VECTOR TO THE NEAREST SUITABLE ARPT. AFTER PERFORMING THE REQUIRED SHUTDOWN ITEMS ON THE CHECKLIST; WE DECIDED TO ATTEMPT A RESTART. ON THE SECOND TRY; THE ENG RELIT AND CAME BACK ONLINE. THE ENG EXHIBITED NORMAL INDICATIONS. AFTER ASSESSING THE SIT; THE FO AND MYSELF DETERMINED THE FLT COULD BE CONTINUED TO THE INTENDED ARPT. A NORMAL TWO ENG APCH AND LNDG WAS MADE AT OUR DESTINATION; WITHOUT ANY COMPLICATIONS. ATC WAS VERY HELPFUL AND ASSISTED US IN A PROFESSIONAL AND EFFICIENT MANNER FOR THIS EVENT. SIX DAYS LATER; OUR FLT CREW SKILLS WERE PUT TO THE TEST AGAIN. REPAIR WORK HAD BEEN COMPLETED ON THE #1 L ENG AFTER EXPERIENCING A FLAMEOUT. EVERYTHING CHECKED OUT AND WAS SIGNED OFF BY THE REPAIR FACILITY. WE FLEW UNEVENTFULLY THE NEXT COUPLE OF DAYS; BUT THE ENG NEVER SOUNDED QUITE RIGHT. I RELAYED THIS TO OUR MECHANICS AND THEY INFORMED US TO KEEP AN EYE ON THE ENG GAUGES. WE DEPARTED ZZZ1 ARPT AND LEVELED OFF AT FL390 ON OUR WAY TO ZZZ2. APPROX 45 MINUTES INTO THE FLT; THE ACFT SEEMED TO HAVE SOME VIBRATION IN THE AIRFRAME. SHORTLY AFTER NOTICING THIS WE HEARD A LOUD BANG AND THE L ENG SPOOLED DOWN. ONCE AGAIN; WE HAD LOST THE #1 ENG; TWICE IN A WEEK! I DISENGAGED THE AUTOPLT AND YAW DAMPER AND RETRIMMED THE ACFT. WE RAN THE ENG SHUTDOWN CHECKLIST AND ASKED ATC FOR PRIORITY HANDLING AND A DSCNT. WE LEVELED AT FL250 AND ATTEMPTED THE FIRST RESTART PROC WITHOUT ANY SUCCESS. WE DECIDED TO ASK ATC FOR A LOWER ALT AND A VECTOR TO THE NEAREST SUITABLE ARPT ZZZ. AFTER LEVELING AGAIN AT FL180; WE ATTEMPTED ONE MORE RESTART. AFTER RUNNING THE CHECKLIST AND TRYING AGAIN; THE ENG FAILED TO RESTART. WE DECIDED TO DIVERT TO ZZZ AND INFORMED ATC WE WOULD LIKE VECTORS TO THE ACTIVE RWY. ATC OBSERVED VERY LITTLE TFC IN THE AREA AND GAVE US OUR RWY OF CHOICE. WE DISCUSSED THE SINGLE ENG PROCS AND PREPARED THE ACFT FOR THE APCH. WITH GOOD WEATHER PRESENT AT OUR ARPT; VERY LITTLE AIR TFC IN THE AREA; AND GREAT SERVICE FROM ATC; WE MADE AN UNEVENTFUL LNDG AT ZZZ. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ENG HAD BEEN IN LONG-TERM STORAGE AND THE COMPRESSOR SEALS HAD BEEN DAMAGED WHILE IN STORAGE. THE RPTR SAID THESE WERE THE COMPONENTS THAT MAINT RPTED HAD FAILED.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.