B737-500 CREW HAD SMOKE ENTER THE CABIN AFTER TURNING UP THE CABIN TEMP. A PAX CALLED 'FIRE' AND BEGAN AN EVAC.

Date: 2004-12 · Aircraft: B737-500

Anomalies: aircraft-equipment-problem-critical|deviation-discrepancy-procedural-far|deviation-discrepancy-procedural-published-material-policy|flight-deck-cabin-aircraft-event-other-unknown|flight-deck-cabin-aircraft-event-smoke-fire-fumes-odor|inflight-event-encounter-other-unknown|inflight-event-encounter-weather-turbulence

Synopsis

B737-500 CREW HAD SMOKE ENTER THE CABIN AFTER TURNING UP THE CABIN TEMP. A PAX CALLED 'FIRE' AND BEGAN AN EVAC.

Narrative

FLT WAS ABOUT 3 HRS LATE DUE TO WX DELAYS AND MECHANICAL PROBS WITH THE ACFT PACKS. PAX WERE BOARDED AND THE JETBRIDGE WAS WITHDRAWN FROM THE ACFT. THE DE-ICE CREW INFORMED US THAT WE HAD A LITTLE RIME ICE ON THE TAIL THAT THEY WANTED TO SPRAY. I CONFIGURED THE ACFT FOR DE-ICING BY ROLLING THE TRIM FULL FORWARD; CLOSING THE APU BLEED VALVE AND CLOSING THE PACK VALVES. WHEN DE-ICING WAS COMPLETE AND WE WERE PREPARING TO PUSH; I RECONFIGURED THE ACFT FOR TKOF AND BECAUSE THE CABIN WAS NOW SO COLD; I PUT THE R PACK ON HIGH AND TURNED THE TEMP UP TO HELP WARM IT UP. THICK SMOKE STARTED TO COME OUT OF THE DE-FOG VENTS; AND THE COCKPIT VERY RAPIDLY BEGAN TO FILL. AT THE SAME TIME; SHOUTS WE HEARD FROM THE CABIN AND I HEARD SOMEONE YELL 'FIRE.' THE PURSER CALLED THE COCKPIT WITH A SERIES OF RAPID CHIMES; AND I HEARD HER YELL TO THE PAX TO EVAC THE ACFT. AT THAT TIME I HEARD THE EVAC SLIDE DEPLOY AND THE PURSER YELL HER COMMANDS TO THE PAX TO JUMP DOWN THE SLIDE. THE CAPT AND I RAN THE EVAC CHKLIST FROM THE QRC. WHEN I WENT BACK TO THE CABIN; ALL THE PAX WERE OUT OF THE ACFT AND THE SMOKE HAD CLRED. ONLY THE SLIDE AT 1L WAS DEPLOYED AND AN OVERWING EXIT ON THE R SIDE WAS OPEN; ALTHOUGH NO PAX APPARENTLY WENT OUT THAT WAY. NO CREW MEMBERS EVACED WHEN IT WAS DETERMINED THAT THE ACFT WAS IN NO DANGER AND THE PAX WERE HERDED TOWARDS THE TERMINAL BY THE GND PERSONNEL. NO INJURIES WERE RPTED AS A RESULT OF THE EVAC. SUPPLEMENTAL INFO FROM ACN 640727: THE L TEMP CTL WAS INOP IN AUTO AND MANUAL. THIS MEANT NO HEAT FOR THE FORWARD PART OF THE CABIN AND COCKPIT. MAINT THEN CHANGED THE WRONG PART; THE R INSTEAD OF THE L. BY THE TIME THE ACFT WAS FIXED IT WAS 3 HRS LATER. THE CAPT ASKED IF THEY WERE ALL DONE AND THE GND PERSON STATED YES. THE CAPT THEN ORDERED THAT THE ACFT BE RECONFIGURED. THE FO PERFORMED THE RECONFIGURING AS THE CAPT FOLLOWED THE DE-ICE CHKLIST. WHEN THE FO TURNED ON THE BLEED SWITCH THE COCKPIT FOGGED OVER. AT THIS TIME A PAX IN THE CABIN YELLED 'FIRE;' DUE TO FOG IN THE CABIN. PEOPLE JUMPED UP AND STARTED FOR THE EXITS. AFTER THE PAX YELLED FIRE; THE CAPT HAD TO ASSUME THAT WAS THE CASE. EVERYONE EVACED THE ACFT WITHOUT INJURIES. RAMP CREWS WERE AT THE BOTTOM OF THE SLIDE TO HELP PEOPLE OFF AND AWAY.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.