A B737-700 CREW EXPERIENCED AN AILERON DEAD BAND BTWN PLUS OR MINUS 0-4 DEGS OF AILERON MOVEMENT. NORMAL INPUT BEYOND 4 DEGS.

Date: 2005-05 · Aircraft: B737-700

Anomalies: aircraft-equipment-problem-critical|other-excessive-aileron-control-free-play

Synopsis

A B737-700 CREW EXPERIENCED AN AILERON DEAD BAND BTWN PLUS OR MINUS 0-4 DEGS OF AILERON MOVEMENT. NORMAL INPUT BEYOND 4 DEGS.

Narrative

IT WAS THE FO'S LEG FROM ZZZ. UPON ROTATION DURING TKOF WITH AN APPROX 15 KT L XWIND; THE FO NOTICED A SIGNIFICANT ROLL DUE TO UNRESPONSIVE AILERON INPUT FOR XWIND CORRECTION. THE FO RECOVERED BY USING R AILERON AND RIGHTING THE WINGS. THE FO THEN TOLD ME THE AILERONS SEEMED 'SLOPPY' AND ASKED ME TO TRY FLYING IT AT APPROX 1200 FT AGL. I TOOK CTL OF THE ACFT AND NOTICED THE SAME THING. BASICALLY THE AILERONS FELT AS THOUGH THERE WAS A DEAD BAND BTWN 4 DEGS L AND R DEFLECTION. ONCE I CONTINUED ROLL INPUT BEYOND 4 DEGS; THE CTLS THEN FELT MORE NORMAL; AND ROLL WAS CTLABLE BEYOND THE 4 DEG POINT. THE ACFT REMAINED IN POSITIVE CTL THROUGHOUT THE FLT; THE AILERONS JUST FELT UNRESPONSIVE IN THIS 4 DEG RANGE OF MOTION EITHER SIDE OF CTR. WE CLBED TO 10000 FT AND DISCUSSED THE PROB. I CHKED CIRCUIT BREAKERS AND DID SOME TROUBLESHOOTING BUT COULD NOT FIND A SOLUTION TO THE PROB. WE THEN DECIDED TO DECLARE AN EMER AND RETURN TO ZZZ. I COMMUNICATED WITH THE FLT ATTENDANTS; OPS AND MAINT WHILE THE FO FLEW. I THEN TOOK OVER CTL OF THE ACFT AND MADE A NORMAL APCH AND LNDG IN ZZZ ON RWY 25. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: RPTR STATED THAT THE AILERON TRIM ACTUATOR WAS REPLACED AND SEVERAL DAYS LATER THE AILERON CTRING BEARING WAS REPLACED. NO FURTHER DISCREPANCIES WERE WRITTEN AGAINST THE AILERON CTL SYS.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.