TEMPORARILY DISTR DURING ENG START ON PUSHBACK; B737 FLT CREW EXPERIENCES HOT START AND EXCESSIVE EGT.
Synopsis
TEMPORARILY DISTR DURING ENG START ON PUSHBACK; B737 FLT CREW EXPERIENCES HOT START AND EXCESSIVE EGT.
Narrative
DURING PUSHBACK AND STARTING THE #2 ENG; THE START EGT WAS EXCEEDED. I WAS LISTENING TO THE PUSHBACK DRIVER; THE COPLT; GND CTL; AND ANOTHER COMPANY AIRPLANE THAT WAS WAITING OUT FOR OUR GATE. WHILE TRYING TO CONCENTRATE ON ALL THESE TASKS; I SENSED SOMETHING WAS WRONG WITH THE ENG START. AT FIRST I TOOK ASSESSMENT OF ALL OF THE ENG GAUGES; BUT ALL SEEMED NORMAL EXCEPT THAT THE ACCELERATION WAS SLOW. SO I SUSPECTED THAT THE FO MAY HAVE LEFT THE PACK ON WHILE STARTING THE ENG. I LOOKED UP TO VERIFY PROPER POS OF THE PACK AND BLEED SWITCHES AND THEN LOOKED BACK AT THE ENG GAUGES. WHEN I LOOKED BACK DOWN AT THE ENG GAUGES; EVERYTHING LOOKED OK EXCEPT THE EGT. THE EGT WAS OVER 800 DEGS C. I CUT THE FUEL AND CHKED TO SEE IF THE START SWITCH HAD CUT OUT. IT HAD NOT. WE MOTORED THE ENG FOR THE REQUISITE 60 SECONDS AND THE FO RAN THE ABORTED ENG START CHKLIST. I RETURNED TO THE GATE; CALLED MAINT AND WROTE UP THE EXCEEDANCE. I ESTIMATE THAT THE PEAK EGT WAS OVER 820 DEGS. I WAS FOCUSED ON THE ENG START AND DISTR AT THE SAME TIME. I CAN'T BELIEVE THAT THERE WAS NO MORE HINTS OF AN IMPENDING HOT START. NO ABNORMAL N1; N2; OR FUEL FLOW. AND I CAN'T BELIEVE I DIDN'T NOTICE THE EGT UNTIL IT WAS TOO LATE. IN THE FUTURE; I WILL REDOUBLE MY EFFORTS TO KEEP ONE EYE ON THE EGT UNTIL ROLLBACK.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.