MD80 FLIGHT ATTENDANT REPORTS THE ACTIVATION OF A LAV SMOKE DETECTOR WHICH RESULTS IN A DIVERSION.

Date: 2006-12 · Aircraft: MD-80 Series (DC-9-80) Undifferentiated or Other Model · Phase: initial_climb

Anomalies: aircraft-equipment-problem-less-severe|flight-deck-cabin-aircraft-event-smoke-fire-fumes-odor

Synopsis

MD80 FLIGHT ATTENDANT REPORTS THE ACTIVATION OF A LAV SMOKE DETECTOR WHICH RESULTS IN A DIVERSION.

Narrative

DURING THE BOARDING PROCESS THE (LAVATORY ON ACFT L AFT) SMOKE ALARM CHIMES STARTED GOING OFF. NO ONE WAS IN THAT LAVATORY. AFTER A FEW MINS (NO MORE THAN 2) IT CEASED. THERE DIDN'T SEEM TO BE ANY ODOR AT THAT TIME AND NO SMOKE WAS VISIBLE. I THOUGHT MAYBE IT WAS SET OFF BY A BLACKBERRY CELL PHONE'S RADIO SIGNALING BUT NO ONE IN THE REAR OF THE ACFT OWNED UP TO HAVING A BLACKBERRY DEVICE. DURING THE DEMO: A FEW MINS LATER; THE CHIMING OF THAT LAVATORY SMOKE DETECTOR STARTED AGAIN; LASTED ABOUT A TOTAL OF 5 MINS -- IT WOULD STOP THEN START UP AGAIN FOR A BRIEF FEW SECONDS THEN STOP. I BELIEVE; CAN'T REMEMBER FOR SURE; THAT THE CAPT CALLED US ABOUT THE ALARM; BUT SINCE THERE WAS NO ODOR AND NO VISIBLE SIGNS OF SMOKE; WE ALL THOUGHT IT WAS MALFUNCTIONING. I CAN'T RECALL HOW MANY TIMES THIS INTERMITTENT 'CHIMING' OCCURRED; BUT BY THE TIME WE WERE STARTING OUR BEVERAGE SVC IT BEGAN AGAIN -- THIS TIME CONTINUOUSLY. THE #4 AND I LOOKED FOR THE SWITCH TO TURN OFF THE ALARM; BUT COULD NOT FIND ONE. THIS PARTICULAR ACFT APPEARED TO HAVE BEEN 'REVAMPED' OR RECONFIGURED AND THE ORIGINAL SHUTOFF TO THE ALARM HAD BEEN DISENGAGED. AFTER LOOKING THE LOCATION UP IN OUR MANUAL WE WERE STILL NOT ABLE TO FIND A SHUTOFF. I THEN DECIDED TO CHK WITH THE CAPT TO SEE IF THEY KNEW AND HE SAID THEY DIDN'T HAVE THAT INFO OR SOMETHING TO THAT EFFECT BUT DID VERIFY WITH US THAT THERE WAS NO SMOKE DETECTED BY VISUAL OR SMELL. ABOUT THAT TIME; A FURLOUGHED OR MAYBE A 'CALLED BACK TO DUTY' FORMER PLT OF OURS WHO WAS TRAVELING WITH HIS FAMILY IDENTED HIMSELF AS ONE OF OUR PLTS OFFERED TO SEE IF HE COULD LOCATE THE SHUTOFF AND AT LEAST KEEP AN EYE ON THE LAVATORY SO WE COULD CONTINUE WITH THE SVC. BY THIS TIME WE HAD ALREADY BLOCKED OFF THE LAVATORY. WITHIN A FEW MINS HE DETECTED WHAT SEEMED TO BE AN ELECTRICAL BURNING ODOR SO HE TURNED THE AIR VENT OFF IN THE LAVATORY. WHEN I RPTED TO THE CAPT THAT THIS PLT SMELLED THE ODOR I WENT BACK IN TO CHK IT MYSELF. NOT KNOWING HE HAD TURNED THE AIR VENT OFF; I TURNED IT BACK ON AND THEN IMMEDIATELY SAW A FAINT PUFF-LIKE CLOUD WHICH QUICKLY DISSIPATED. WE INFORMED THE CAPT ABOUT THE STRENGTHENING ELECTRICAL BURNING ODOR AND SMOKE-LIKE BRIEF 'PUFF' AND HE MADE THE DECISION TO DIVERT FOR FURTHER INVESTIGATION ON THE GND. THE FINAL CONSENSUS ON THE GND WAS THAT THE OXYGEN MASK IN THE LAVATORY WAS DISENGAGED/ACTIVATED WHICH EMITTED THE ODOR AND VAPOR. WE CONTINUED ON TO ZZZZ.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.