HEAVY FREIGHT ACFT WAS AWAITING TKOF CLRNC AND ANOTHER ACFT REPORTED AN ENG FIRE ON THE FREIGHTER. AFTER THE ENG FIRE PROCEDURE WAS ACCOMPLISHED; FIRE WAS STILL REPORTED; SO THE FLT CREW EVACUATED THE ACFT.
Synopsis
HEAVY FREIGHT ACFT WAS AWAITING TKOF CLRNC AND ANOTHER ACFT REPORTED AN ENG FIRE ON THE FREIGHTER. AFTER THE ENG FIRE PROCEDURE WAS ACCOMPLISHED; FIRE WAS STILL REPORTED; SO THE FLT CREW EVACUATED THE ACFT.
Narrative
THIS EVENT INVOLVED AN ENG FIRE DURING TAXI OUT. 4 ENG START WAS NORMAL. TAXI OUT OF RAMP WAS NORMAL. A DISTR ON TAXI TO RWY XXL WAS A RADAR MALFUNCTION. THE CAPT USED RAMP TO GET OUT OF THE TFC FLOW AND DIAGNOSE THE PROB. ENGS #1 AND #4 WERE SHUT DOWN FOR FUEL CONSIDERATIONS. THE RADAR BECAME OPERATIVE AND THE CAPT RE-ENTERED THE TAXI STREAM. THE BEFORE TKOF CHKLIST WAS INITIATED FROM THE TOP; AGAIN. ENG STARTS ON ENGS #1 AND #4 WERE NORMAL. AS WE SAT AT THE #1 POS FOR TKOF; ANOTHER ACFT RPTED AN ENG FIRE ON AN ACFT AT RWY XXL. THE CAPT QUERIED THE XMISSION TO DETERMINE IF OUR ACFT WAS THE ONE BEING REFERRED TO. IT WAS; AND THE OTHER ACFT SUGGESTED THAT THE 'TORCH' WAS ABOUT 3-4 FT LONG AND ON THE R INBOARD ENG. DURING THIS TIME OUR CREW AND THE MAINT SUPVRS ON BOARD COULD SEE NO UNUSUAL INDICATIONS OF ENG MALFUNCTION OR FIRE. AFTER ENG #3 WAS SHUT DOWN AND FIRE AGENT DISCHARGED; THE OTHER ACFT CREW CONFIRMED THAT THE 'TORCH' STILL EXISTED. THE CAPT DECIDED THAT AN EMER EVAC WAS APPROPRIATE AND WAS ACCOMPLISHED. ALL EQUIP WORKED NORMALLY; THE EVAC WAS SMOOTH AND THERE WERE NO INJURIES. WE ACCOUNTED FOR EVERYONE (7 SOULS) AND GATHERED IN FRONT OF THE ACFT UNTIL EMER SVCS ARRIVED. EVEN THOUGH I HAD REVIEWED OPS LIMITS AND EMER PROCS ON THE COMMUTE TO WORK; I SHOULD HAVE TESTED FOR FIRE DETECTION SYS FAILURE DURING THE INCIDENT. ALSO; I FOUND MYSELF UNCOMFORTABLE WHEN FIRING THE FIRE AGENT AND I SHOULD HAVE BEEN BETTER AT CHALLENGE; RESPONSE; RESPONSE ALTHOUGH IT MAY NOT HAVE BEEN THAT IMPORTANT ON THE GND. THE CREW PERFORMED WELL TOGETHER; THE CAPT MADE GOOD WELL CONSIDERED DECISIONS AND THE MAINT SUPVRS WERE HELPFUL AND FOLLOWED DIRECTIONS WELL. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THIS WAS A NIGHT FLT WITH RAIN FALLING AT THE ARPT. THE REPORTER INDICATED THAT THEY HAD MADE THE TURN TO HOLD SHORT OF THE RWY; AND THE REPORTING ACFT WAS STILL ON THE PARALLEL TXWY. AS A RESULT; THE REPORTING ACFT WAS LOOKING DOWN THE WING AND ACTUALLY REPORTED A FIRE FOR THE WRONG ENG. THE #4 ENG WAS ACTUALLY PRODUCING THE FLAME. A DEFECTIVE FUEL/OIL HEAT EXCHANGER WAS DISCOVERED. THIS RESULTED IN A MIXTURE OF FUEL AND OIL BEING DISTRIBUTED TO THE ENG BEARINGS.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.