GII FO REPORTS STEERING MALFUNCTION ON TAXI OUT DUE TO IMPROPERLY INSTALLED NOSE GEAR STEERING PIN.

Date: 2008-06 · Aircraft: Gulfstream II (G1159) · Phase: taxi

Anomalies: aircraft-equipment-problem-critical|deviation-discrepancy-procedural-maintenance|ground-event-encounter-loss-of-aircraft-control

Synopsis

GII FO REPORTS STEERING MALFUNCTION ON TAXI OUT DUE TO IMPROPERLY INSTALLED NOSE GEAR STEERING PIN.

Narrative

WHILE TAXIING ON TXWY H IN PREPARATION FOR TKOF; THE ACFT BEGAN TO SHUDDER VIOLENTLY AND THE CAPT RPTED A LOSS OF NOSEWHEEL STEERING. AS THE ACFT CAME TO A STOP; STILL ON TXWY H BUT OFF OF THE CTRLINE; THE CAPT SET THE PARKING BRAKE. THE FLT ATTENDANT CAME TO THE COCKPIT TO INQUIRE ON THE ACFT STATUS. A CHK FROM THE CREW IN BOTH THE COCKPIT AND OUTSIDE (THROUGH WINDOWS) YIELDED NO REQUIREMENT TO EVAC THE PAX. FEARING THAT THERE MAY BE AN UNSEEN ISSUE WITH THE LNDG GEAR; THE CAPT ELECTED TO OPEN THE AIRSTAIR DOOR AND VISUALLY INSPECT THE EXTERIOR OF THE ACFT. PRIOR TO; AND DURING THE CAPT'S INSPECTION; I ATTEMPTED TO NOTIFY ZZZ GND CTL OF OUR SITUATION. I BELIEVE THAT DUE TO THE SHAKING OF THE ACFT AND LOUD AMBIENT NOISE (ENG AS WELL AS PAX) I WAS UNABLE TO XMIT FROM THE FO POS ON BOTH COM #1 AND COM #2. THE CAPT RETURNED TO THE FLT DECK AND NOTIFIED US THAT A PIN CONNECTING THE NOSEWHEEL STEERING HAD COME OUT; AND WE HAD A LOSS OF STEERING. THE PIN WAS RECONNECTED AND STEERING WAS ESTABLISHED. I ALERTED THE CAPT TO OUR LOSS OF COM. AN ARPT WORKER CONTACTED THE CAPT AND WE RETURNED TO THE FBO FOR A FURTHER INSPECTION. I WAS UNABLE TO XMIT FROM THE FO POS UNTIL I DISCOVERED THAT THE 'PUSH-TO-TALK' SWITCH WAS STICKING; NOT ALLOWING A COMPLETE XMISSION. MOST LIKELY AS A RESULT OF THE ACFT SHAKING. THE CAPT WAS ABLE TO XMIT FROM HIS POS. WE DISCOVERED THAT UNKNOWN GND PERSONNEL HAD 'PINNED' THE LNDG GEAR AND INCORRECTLY RECONNECTED THE NOSEWHEEL STEERING WITHOUT THE CREW PRESENT. DUE TO THE SIZE OF THE PIN; AND ITS LOCATION; THE CAPT DID NOT NOTICE THAT THE PIN WAS SEATED INCORRECTLY AND THAT THE COTTER PIN USED TO SECURE THE MAIN PIN (AS A SAFETY BACK-UP) WAS NOT INSTALLED CORRECTLY. NO INJURIES TO PERSONS OR DAMAGE TO THE ACFT OCCURRED.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.