AN A321 PILOT REPORTS; THAT WHEN STARTING THE APU FOR ELECTRICS; THE APU BLEED AIR CAME ON WITHOUT BEING SELECTED. THIS ALSO CAUSED THE #1 AND #2 ENG IP AND HP BLEED VALVES TO STAY CLOSED AFTER ENG START.
Synopsis
AN A321 PILOT REPORTS; THAT WHEN STARTING THE APU FOR ELECTRICS; THE APU BLEED AIR CAME ON WITHOUT BEING SELECTED. THIS ALSO CAUSED THE #1 AND #2 ENG IP AND HP BLEED VALVES TO STAY CLOSED AFTER ENG START.
Narrative
UPON ARR AT THE ACFT; I SAW THAT MEL 36-12-01 BLEED AIR SUPPLY SYS WAS APPLIED ON THE ACFT. THE ONLY CREW ACTION IS TO CHK PLACARDING PROCS. THE APU BLEED AIR WAS MEL'ED BECAUSE THE COVER ON THE RESPECTIVE PUSH BUTTON HAD FALLEN OFF. THE PUSH BUTTON COVER WAS ON AND HAD BEEN REATTACHED IN SOME MANNER. WHEN WE STARTED THE APU FOR ELECTRICS; WE NOTICED THAT THE APU BLEED AIR CAME ON WITHOUT US SELECTING IT. THIS WAS CONFIRMED BY THE POS OF THE APU BLEED VALVE POS WITH AIR PRESSURE INDICATION ON BOTH THE APU AND BLEED PAGES. I ATTEMPTED TURNING OFF THE APU BLEED AIR; BUT THE PUSH BUTTON FELT LIKE IT WAS NOT ENGAGING. NOTHING WE DID WOULD SHUT OFF THE APU BLEED AIR. I SHUT DOWN THE APU AND CALLED THE DISPATCHER WHO GOT MAINT CTL ON THE PHONE. MAINT CTL SAID THAT THE MEL WOULD HAVE TO BE RECLASSIFIED AND A MECH CAME OUT AND APPLIED MEL 36-12-02 APU BLEED VALVE; WHICH REQUIRES THAT MAINT MANUALLY SECURE THE BLEED VALVE SHUT. THIS WAS DONE; HOWEVER THE MECH STATED THAT THE BLEED VALVE MAY INDICATE OPEN ON THE SYS PAGES IN THE COCKPIT. (I CAN'T REMEMBER IF HIS SOURCE FOR THIS STATEMENT WAS MAINT CTL OR MEL REF MATERIALS HE HAD AVAILABLE BEYOND WHAT IS IN THE COCKPIT.) WE FINALLY STARTED #1 ENG USING EXTERNAL ELECTRICS AND AN AIR CART; WITH PLANS TO DO A XBLEED START AFTER PUSHBACK. MIND YOU NOW; TEMPS IN THE CABIN ARE APCHING 100 DEGS. DURING THE XBLEED PROC; WE NOTICED THAT BOTH THE #1 ENG INTERMEDIATE PRESSURE AND HIGH PRESSURE BLEED VALVES WERE CLOSED. WE INCREASED PWR SLIGHTLY ON THE #1 ENG WITH NO CHANGE IN BLEED AIR SUPPLY. I HAD FELT FROM THE BEGINNING THAT WITH THE APU BLEED VALVE INDICATING OPEN THAT THE ENG BLEEDS WOULD NOT OPEN; AND SINCE THE CABIN TEMP WAS BECOMING UNBEARABLE; I HAD THE GND CREW TOW US BACK IN TO THE GATE AND I INSTRUCTED THE GATE AGENT TO IMMEDIATELY DEPLANE THE PAX UNTIL THE MAINT SITUATION WAS RESOLVED. SEVERAL MECHS STARTED THE #1 ENG AND RECEIVED THE SAME BLEED INDICATIONS WE HAD GOTTEN. THEY FINALLY DECIDED TO CHANGE THE PANEL CONTAINING THE APU BLEED AIR PUSH BUTTON AND THE PROB WAS SOLVED. MEL WAS REMOVED AND WE DEPARTED ABOUT 2 HRS LATE. I RECOMMEND THAT THE APU BLEED MEL'S BE REVIEWED FOR ACCURACY REGARDING ACTUAL OP. EVEN THOUGH THE APU BLEED VALVE WAS MANUALLY CLOSED; THE SIGNAL TO THE VALVE (ASSUMED TO BE FROM THE PUSH BUTTON) SHOWED THE VALVE OPEN WITH BLEED AIR BEING SUPPLIED. THIS THEN PREVENTED THE ENG BLEEDS FROM OPENING.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.