A DASH 8 Q200'S ENG FAILED BENIGNLY DURING DSCNT FOR LNDG. AN EMER WAS DECLARED FOLLOWED BY AN UNEVENTFUL LNDG.

Date: 2008-08 · Aircraft: Dash 8-200 · Phase: descent

Anomalies: aircraft-equipment-problem-critical

Synopsis

A DASH 8 Q200'S ENG FAILED BENIGNLY DURING DSCNT FOR LNDG. AN EMER WAS DECLARED FOLLOWED BY AN UNEVENTFUL LNDG.

Narrative

INITIALLY DURING OUR DSCNT FROM 16000 FT MSL ON OUR WAY TO ZZZ AT ROUGHLY 15000 FT MSL; THE EVENT OCCURRED. WE WERE IN ICING CONDITIONS; BUT NO ICE WAS ACCUMULATING. WE WERE IN VERY LIGHT TURB AT THE TIME AS WELL. THE EVENT STARTED AS THE #1 TORQUE GAUGE SLOWLY BLEEDING OFF. (WE WERE AT A PWR SETTING OF ROUGHLY 90% TORQUE AT THE TIME.) THEN WE NOTICED THE #1 FUEL FLOW GAUGE ALSO BLEEDING OFF. (WE WERE AT A FUEL FLOW OF ROUGHLY 650 PPH.) AT ROUGHLY 25% TORQUE AND 250 PPH FUEL FLOW; WE NOTICED A SLIGHT YAW BEGINNING TO OCCUR AND I CALLED FOR THE #1 ENG FAILURE CHKLIST. WE RAN THE CHKLIST; SHUT DOWN THE #1 ENG; AND DECLARED AN EMER. (ADDITIONAL CHKLIST RAN WERE THE ENG CLEANUP ITEMS CHKLIST AND THE SINGLE ENG LNDG CHKLIST AND ITS ASSOCIATED PARTS.) WHILE BTWN CHKLISTS; I INFORMED OUR FLT ATTENDANT; 'WE HAD AN ENG FAILURE. WE ARE PLANNING A NORMAL DEPLANING AFTER WE SHUT DOWN ON THE RWY AND DEPLANE. WE HAD JUST OVER 5 MINS FOR HER TO GET READY. AND THAT WE WOULD GET BACK TO HER PRIOR IN ABOUT 5 MINS.' I ALSO REASSURED HER THAT THE ACFT WAS ALRIGHT; OTHER THAN THE FAILED ENG. WE RAN ASSOCIATED CHKLISTS; GOT A HOLD OF DISPATCH AND OPS; AND PROCEEDED IN FOR A SINGLE ENG ILS APCH. WE SHOT THE ILS APCH AND LANDED UNEVENTFULLY. WE PROCEEDED TO SHUT DOWN ON THE RWY WITH CRASH; FIRE; RESCUE ALREADY ON SCENE. THIS TOOK A FEW MOMENTS TO COLLECT OUR THOUGHTS AND SHUT DOWN THE #2 ENG; DUE TO AN EXCESS AMOUNT OF ADRENALINE FLOWING. AFTER CRASH; FIRE; RESCUE ASSURED US THE ACFT WAS SECURE; WE SHUT THE ACFT DOWN; I OPENED THE FLT DECK DOOR; SPOKE BRIEFLY TO THE PAX (APOLOGIZING FOR EXCITING EVERYONE; ASSURING THEM EVERYTHING WAS OK; AND INFORMING THEM IT WOULD BE A FEW MORE MOMENTS AND WE WOULD BE TOWED IN). I OPENED THE MAIN CABIN DOOR; SPOKE TO THE CRASH; FIRE; RESCUE INCIDENT COMMANDER BRIEFLY; AND TALKED FACE-TO-FACE WITH THE ZZZ ACR ESCORT TEAM; TOW TEAM. WE WERE TOWED IN UNEVENTFULLY AND PAPERWORK -- PHONE CALLS ENSUED. AS A SIDE NOTE; WE CHOSE TO SHUT DOWN ON THE RWY BECAUSE: 1) WE WANTED TO MAKE SURE THAT IF WE HAD INADVERTENTLY MISSED ANYTHING DUE TO EXCESS ADRENALINE; WE WOULD NOT HAVE AGGRAVATED THE SITUATION TRYING TO DO TOO MUCH OR 2) IF WE HAD INADVERTENTLY MISSED ANYTHING DUE TO HAVING JUST PREVIOUSLY COMPLETED A 12 HR DAY WITH A 9 HR OVERNIGHT.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.