B767 FLIGHT CREW REPORT INBOARD AILERON STUCK IN THE 50% UP POSITION AFTER TAKE OFF. EICAS FLIGHT CONTROL DISPLAY INDICATES THAT AILERON DOES NOT MOVE IN TURNS. COMMUNICATION DIFFICULTIES PREVENT MAINTENANCE INVOLVEMENT AND PROBLEM CORRECTS ITSELF.
Synopsis
B767 FLIGHT CREW REPORT INBOARD AILERON STUCK IN THE 50% UP POSITION AFTER TAKE OFF. EICAS FLIGHT CONTROL DISPLAY INDICATES THAT AILERON DOES NOT MOVE IN TURNS. COMMUNICATION DIFFICULTIES PREVENT MAINTENANCE INVOLVEMENT AND PROBLEM CORRECTS ITSELF.
Narrative
DURING TAXI OUT; THE FLT CTLS TESTED NORMALLY AFTER FLAP EXTENSION. ON INITIAL CLB; I NOTICED AN UNUSUAL L ROLL TENDENCY WHICH WAS EASILY CORRECTED WITH OPPOSITE ROLL INPUT. AFTER WE CLEANED UP AND WERE ESTABLISHED ON COURSE; I ATTEMPTED TO CORRECT WITH RUDDER TRIM AS NORMAL. A SUBSTANTIAL AMOUNT OF TRIM WAS REQUIRED TO REDUCE THE L ROLL TENDENCY. AFTER LEVELING AT FL300; WE DISCUSSED THE OUT OF TRIM SITUATION AND WORKED TO RE-TRIM USING FLT MANUAL PROCS. THE EICAS DISPLAY SHOWED THE L INBOARD AILERON IN THE 50% UP POS AND NOT RESPONDING TO CTL INPUTS IN COORD WITH THE R INBOARD AILERON. CAPT THEN NOTIFIED MAINT CTL OF THE TRIM SITUATION AND ATTEMPTED TO CONTACT DISPATCH VIA SATCOM. COMS WITH DISPATCH AND MAINT CTL BECAME AN EXERCISE IN FUTILITY DUE TO FAILING SATCOM VOICE AND ACARS AND VERY POOR HF COMS. WE DISCUSSED OUR OPTIONS AND CHOSE TO CONTINUE TO ZZZ WHILE CAREFULLY MONITORING OUR FUEL STATE AT EACH WAYPOINT. APPROX 90 MINS INTO THE FLT THE L AILERON BEGAN TO RETURN TO ITS NORMAL FLARED POS AND THE FLT CTLS WERE RE-TRIMMED AS NORMAL. THE FLT CONTINUED NORMALLY TO ZZZ. CALLBACK CONVERSATION WITH RPTR ACN #809562 REVEALED THE FOLLOWING INFO: ALTHOUGH MAINTENANCE WAS QUITE CURIOUS ABOUT THE AILERON WRITE UP IN THE AIRCRAFT LOG; NO POSSIBLE FAULT SCENARIOS WERE DISCUSSED AND THE REPORTER WAS NEVER INFORMED OF THE FINDINGS.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.