A MD80 crew experienced a violent and severe flight disruption at FL330 caused by a compressor stall. An emergency was declared with a diversion to a nearby airport.

Date: 2009-10 · Aircraft: MD-80 Series (DC-9-80) Undifferentiated or Other Model · Phase: cruise

Anomalies: aircraft-equipment-problem-critical

Synopsis

A MD80 crew experienced a violent and severe flight disruption at FL330 caused by a compressor stall. An emergency was declared with a diversion to a nearby airport.

Narrative

Cruise at FL330; day; clear; smooth. Aircraft experienced a violent and severe event that felt like an impact; like a car accident; with a pitch down and airframe shudder that extended throughout the aircraft. It was one; instant impact that was so severe that I could hear galley items impacting and felt a deceleration. If we had not had our seat belts on it would have tossed us from our seats. I immediately clicked off the autopilot thinking that an engine had exploded. The engine instruments all were normal and steady. I checked the cabin pressure and noted steady and appropriate cabin altitude and differential. I checked the door lights and saw no open door indications. There were no warning lights or caution lights. Since we still had pressurization we concluded it was probably not a bomb; although a bomb would have felt and sounded the same. As we had eliminated all normal system failures we discussed the possibility of a control or airframe malfunction or damage. Captain declared an emergency and selected a nearby airport for landing. Flight attendants called reported no injuries. Captain gave the flight attendants a briefing and a PA to passengers. I began a shallow descent and slowed to 250 KTS in consideration of the possibility of an airframe or control problem and spiraled down to the airport. There was no QRH checklist for these circumstances; so we completed the Descent Checklist and Before Landing Checklist. The Captain took the aircraft on final and made an overweight landing at 135;000 LBS. Rate of descent was 200 FPM and touchdown was smooth. After landing; ARFF inspected the aircraft and found no obvious damage. Taxied to the gate. As we see in the case of a lightning strike; each passenger said it felt like the impact was directly under their seats; no matter where they were sitting. As passengers deplaned they were clearly shaken; but they all had positive attitudes and patience. This must be directly credited to the excellent cabin crew. They had very little to go on but were able to reassure the passengers while going from doing a cabin service to an emergency landing. I concur with all of Captain's decisions and compliment his handling of this event and the care he demonstrated for his crew throughout our time on the ground.

NASA callback

The reporter stated that feeling in the aircraft at the time of the event was like driving a sports car over a 4X4 board at 40 MPH. The entire crew; including the flight attendants considered the experience and everyone agreed that it was different from wake turbulence. The flight crew then considered the possibility of the elevator jackscrew slipping and so began a descent. They were later told the Digital Data Flight Recorder indicated a compressor stall occurred at the time of the event. The reporter stated that all engine and systems indications were normal the remainder of the flight and they did not see the compressor stall on the engine instruments. The engine was subsequently changed.

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.