C150 student pilot reports engine failure approaching his home airport and elected to land on a two lane highway. No damage occurred and the aircraft was repaired and flown back to the home field.
Synopsis
C150 student pilot reports engine failure approaching his home airport and elected to land on a two lane highway. No damage occurred and the aircraft was repaired and flown back to the home field.
Narrative
Descending to ZZZ; at an altitude of approximately 7;500 FT MSL (4;300 FT AGL) and 10 miles from the airport; the engine quit without any advance warning. All engine gauges and instruments had just been checked in conjunction with making the 10-mile inbound radio announcement. Everything was within norms with throttle set at approximately 2;100 RPM for slow descent. Mixture had been leaned at cruise at 8;500 FT approximately 30 minutes earlier. Plane was immediately set for best glide and trimmed. Plane was banked towards two-lane highway about half-mile away. Mixture was set to full rich and engine restart was attempted twice. Each time it ran rough for just a few seconds. On the third attempt engine would only turn over. Emergency radio announcements were made twice on the CATF. After making a couple of shallow turns to look at nearby rough dirt roads; the decision was made to stay with landing on the paved road; even though it was moderately busy with traffic. Though the final few feet of the landing approach was close to the traffic going the same direction; the oncoming traffic easily saw the plane and pulled to the side of the road. There was never a time that the plane could not have been diverted to the relatively flat; though bushy; terrain on the sides of the road if it appeared the cars on the road could not be cleared. Landing was with full flaps. The plane slowed quickly; and was steered down into a slight gully and into some small bushes in order to not remain in traffic. Airport personnel were called immediately to report my status. Two A&Ps drove from the airport and quickly ascertained that the mixture cable had snapped at a point where the cable goes into the carburetor housing. There was nothing to indicate any out-of-the-ordinary wear and stress on the cable; so at this time; it appears to be a defective or weak cable that just broke. Trips were made for parts and to retrieve engine log books. Repair was made; logs were signed to indicate airworthiness; and permission was obtained from the FAA for the Department of Public Safety to block traffic so the plane could be flown out. One of the A&P/Pilots flew the plane the approximate 6 NM flight back to ZZZ without further incident.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.