LGT PLT OVERTEMPED ALL 3 ENGINES DURING TKOF DEN.
Synopsis
LGT PLT OVERTEMPED ALL 3 ENGINES DURING TKOF DEN.
Narrative
OUR GROSS WT WAS APPROX 164000#; ROUGHLY 10000# BELOW THE MAX FOR THAT PARTICULAR TKOF. WE USED RWY 35L AND HAD A LIGHT XWIND FROM THE NW. THE WX WAS CLR AND NO TSTMS WERE IN THE AREA. NO ACFT BEFORE OR AFTER OUR DEP RPTED ANY WIND SHEAR OR OTHER ADVERSE WX CONDITIONS. ENG START AND TAXIOUT WAS NORMAL. IT WAS THE CAPT'S LEG. WE WERE CLRED FOR TKOF AND BEGAN OUR TKOF ROLL. ALL SYSTEMS WERE NORMAL. AFTER VR THE CAPT WAS SLOW TO ROTATE THE NOSE UP. WITH APPROX 1500-2000' REMAINING RWY; THE CAPT FOR NO APPARENT REASON ADVANCED THE THROTTLES WELL FORWARD OF THE MAX TKOF POS. AIRSPD WAS APPROX V2 + 4 KTS AND APPROX 6-7 DEGS NOSE UP ATTITUDE. AFTER WE WERE SAFELY AIRBORNE THE F/O RETARDED THE THROTTLES BACK TO BRING THE EGT BACK TO THE YELLOW BAND FROM ABOVE THE RED BAND; 655-660 DEGS; THERE WERE NO ENG ABNORMALITIES. WE ESTIMATE THE EGT'S WERE AT 655-660 DEGS FOR ABOUT 5 SECS. WE CONTINUED THE CLBOUT. AT THE FIRST OPPORTUNITY THE F/O QUESTIONED THE CAPT ABOUT HIS ACTIONS ON TKOF. HE STATED THAT HE THOUGHT HE HAD ENCOUNTERED A WIND SHEAR. NEITHER THE F/O OR MYSELF NOTICED ANYTHING TO INDICATE WIND SHEAR. WE CONTACTED OUR SYS'S ACFT MAINT CTLR VIA ARINC RADIO AND GAVE HIM ALL THE DETAILS OF THE OCCURRENCE. ALL ENGS APPEARED NORMAL AND HE INDICATED THAT CONTINUING TO OUR DEST WOULD BE APPROPRIATE; HE WOULD PROVIDE ACR MECHS TO COME TO MILWAUKEE TO INSPECT THE ENGS. THE CAPT CONCURRED THAT THE COURSE OF ACTION WAS REASONABLE UNDER THE CIRCUMSTANCES. WE CONTINUED TO MONITOR THE ENGS CLOSELY FOR THE REMAINDER OF THE FLT AND SAW NO ABNORMALITIES WHATSOEVER. WE LANDED AT MILWAUKEE W/O INCIDENT. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING: THE F/O AND S/O SENT RPTS TO COVER THEMSELVES IN CASE SOMEONE WONDERED WHY THEY DID NOT RPT THE WIND SHEAR AT DEN. THE CAPT IS APCHING RETIREMENT. THE CAPT WAS NOT VERY ALERT DURING THE WHOLE TRIP AND ALMOST DOVE INTO THE GND APCHING MKE LATER IN THE SEQUENCE. (4000 FPM DSCNT RIGHT DOWN TO HIS CLRED ALT. HAD TO BE WARNED BY S/O.) S/O IS CONVINCED THAT THE CAPT SUDDENLY BECAME AWARE OF THE END OF THE RWY APCHING AND ADDED PWR AND INCREASED HIS RATE OF ROTATION. HE SAID THAT CAPT THEN HEDGED ABOUT RPTING THE OVERTEMP WORRYING ABOUT HOW MUCH IT WOULD COST THE COMPANY. RPTR SAID THAT CAPT HAD BEEN A SCAB DURING THE RECENT STRIKE BUT HE DIDN'T SEE HOW THIS COULD HAVE ANY EFFECT.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.