ACR MLG ENGINE TAILPIPE FIRE DURING PUSHBACK AND ENGINE START. FO TURNED ON EMERGENCY LIGHTS INSTEAD OF THE ENGINE IGNITION. FUEL WAS INTRODUCED INTO A HOT TAILPIPE AND STARTED TO BURN.
Synopsis
ACR MLG ENGINE TAILPIPE FIRE DURING PUSHBACK AND ENGINE START. FO TURNED ON EMERGENCY LIGHTS INSTEAD OF THE ENGINE IGNITION. FUEL WAS INTRODUCED INTO A HOT TAILPIPE AND STARTED TO BURN.
Narrative
MLG HAD 2 MEL'S ALREADY. FWD AIRSTAIR INOP AND 1 ENG FIRE DETECTOR LOOP. ENRTE TO MSY RIGHT AIR CONDITIONING SUPPLY TEMP HIGH LIGHT ILLUMINATED. LIGHT EXTINGUISHED AFTER I TURNED THE RIGHT HP BLEED OFF. NOTIFIED MY MAINT CENTER IN CHICAGO WHO ARRANGED FOR CONTRACT MAINT TO CHK OUT THE PROB. ABOUT 15 MINS AFTER REFUELING I HAD A FUEL SPILL OUT THE RIGHT WING VENT. A CHECK VALVE HAD UNSEATED ALLOWING THE CENTER FUEL PUMPS TO PUMP FUEL INTO THE LEFT TANK. PLANNED LOAD WAS 9000/5500/9000. GAUGE READ 9600/4500/9000. CALLED MSY FD TO WASH FUEL SPILL AND SECURED ELECTRICAL PWR FROM ACFT. 3 PAX WHO WERE DENIED BOARDING FOR CAUSING A DISTURBANCE AT THE GATE WALKED DOWN THE JETWAY AND HAD TO BE REMOVED BY MSY POLICY. FOLLOWING A MAINT RUN UP OF RIGHT ENG TO CHK ACFT HIGH TEMP LIGHT; WE BOARDED THE ACFT. CONTRACT RAMP PERSONNEL DID NOT UTILIZE A HEADSET DURING PUSHBACK BUT RELIED ON HAND SIGNALS. OUR COMPANY PROC DURING PUSHBACK STARTS IS FOR THE F/O TO FLOW; READ AND RESPOND TO THE ENG START CHKLIST AND THE CAPT TO COORDINATE THE PUSHBACK. THE F/O INADVERTENTLY REACHED UP AND MOVED THE EMER LIGHTS FROM 'ARM' TO 'ON'; INSTEAD OF PUTTING THE IGNITION SWITCH TO 'GND START AND CONTINUOUS'. BOTH SWITCHES ARE THE SAME SIZE AND SHAPE AND ARE LOCATED ABOUT 4' APART. AT 20% N2 HE RPTED NO IGNITION (LIGHT OFF). I SAW THE IGNITION SWITCH WAS OFF. NOW I SAW THE EMER LIGHTS WERE ON. I TOLD HIM TO ABORT THE START AND MOTOR THE STARTER TO CLEAR THE ENG. THE FUEL LEVER WAS OFF AFTER HE ABORTED THE START. I TOLD HIM TO START THE LEFT ENG AND WE WOULD START THE RIGHT AFTER INDICATIONS STABILIZED. AT THIS POINT I NOTICED THE GND CREW WAVING; BUT COULD NOT INTERPRET ANY CLEAR SIGNALS. FINALLY; I UNDERSTOOD THEIR INTENTION; BUT WAS NOT QUITE SURE WHAT ENG HAD THE PROB. ONE OF THE RAMP PERSONNEL CALLED GND CTL TO RPT A SMALL FUEL FIRE IN THE #2 ENG EXHAUST (POOLED FUEL). I IMMEDIATELY MOTORED THE #2 ENG FOR 20 SECS. I OPENED THE COCKPIT WINDOW AND TOLD THE GND CREW TO TOW THE ACFT BACK TO THE GATE. SINCE THE AIRSTAIRS WERE INOP. AFTER BRIEFING THE F/A'S THEY TOLD THE PAX TO DEPLANE AND WAIT IN THE BOARDING AREA. MAINT INSPECTED THE ACFT AND RETURNED IT TO SVC. THERE WAS A DEFINITE PROB IN COM DURING PUSHBACK W/O A HEADSET FOR THE GND CREW. THE HOT EXHAUST STACK FROM THE PREVIOUS MAINT RUN OF THE #2 ENG APPARENTLY IGNITED THE POOLED FUEL.
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.