INFLT ENG FLAMEOUT.
Synopsis
INFLT ENG FLAMEOUT.
Narrative
DURING CRUISE FLT; THE CAPT LEFT THE COCKPIT. A SHORT TIME LATER THE AUTOPLT DISENGAGED AND THE ESSENTIAL PWR FAILURE LIGHT ILLUMINATED. MY FIRST IMPRESSION WAS THAT WE HAD LOST THE #3 GENERATOR; SO I ASKED THE SO IF THAT WAS THE CASE. AT THE SAME TIME; THE CAPT CAME BACK IN AND ASKED WHY ALL OF THE EMER EXIT LIGHTS WERE ON IN THE CABIN. THE NEXT THING I NOTICED WAS THAT THE #3 FUEL FLOW GAUGE READ '0' AND THAT THE ACFT WAS LOSING SPD. AT THAT POINT I STATED THAT WE HAD LOST THE #3 ENG. ALL NECESSARY CHKLISTS WERE ACCOMPLISHED AND A DSCNT AND RETURN TO NGO WAS INITIATED. THE CAPT SAID THAT WHEN HE RETURNED TO THE COCKPIT HE OBSERVED BOTH FUEL BOOST PUMPS IN THE #3 TANK IN THE OFF POS AND THE #3 XFEED VALVE CLOSED ON THE SO'S PANEL. THIS CONFIGN CAUSED THE FUEL STARVATION AND RESULTING FLAMEOUT OF THE #3 ENG. AFTER SOME DISCUSSION; THE #3 ENG WAS RESTARTED AND A NORMAL LNDG WAS ACCOMPLISHED AT NGO. ALL 3 CREW MEMBERS ARE EXPERIENCED B-727 PLTS. THIS FAILURE OCCURRED DURING THE PHASE OF FLT WHEN THE ATMOSPHERE IN THE COCKPIT IS FAIRLY SLOW AND RELAXED AND DURING THE TERMINATION OF A LENGTHY FUEL XFEED PROC. THE SO BECAME DISTRACTED DURING THE TERMINATION OF THE XFEED AND BELIEVED HE HAD ACCOMPLISHED THE PROC CORRECTLY. SUPPLEMENTAL INFO FROM ACN 306129: WE HONESTLY ADMITTED THAT WE HAD CREATED OUR OWN DILEMMA; TOOK CORRECTIVE ACTIONS TO INSURE SAFETY; COMMUNICATED SAME AND CORRECTED THE EMER. CONTRIBUTING TO SEEMING COMPLACENCY AND IMPROPER FUEL MGMNT COULD BE THE SENSE OF FRUSTRATION OUR SO IS FEELING DUE TO FURLOUGH NOTICES RECEIVED AND DOWNSIZING; RECONFIGURING OF THIS AIRLINE WHICH IS EVER ONGOING.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.