ATR42 MECH FAILED TO SECURE OIL FILLER CAP CAUSING LOSS OF OIL AND LOW OIL PRESSURE ON TKOF. TKOF ABORTED. RETURNED TO GATE FOR SVC. THIS GATE DEP AND RETURN WAS NOT NOTED IN THE LOGBOOK NOR WAS THE NEED FOR SVC AND THE ABORTED TKOF.
Synopsis
ATR42 MECH FAILED TO SECURE OIL FILLER CAP CAUSING LOSS OF OIL AND LOW OIL PRESSURE ON TKOF. TKOF ABORTED. RETURNED TO GATE FOR SVC. THIS GATE DEP AND RETURN WAS NOT NOTED IN THE LOGBOOK NOR WAS THE NEED FOR SVC AND THE ABORTED TKOF.
Narrative
WE HAD TAXIED OUT ABOUT 1 1/2 HRS LATE DURING A SNOWSTORM. WHEN WE WERE CLRED FOR TKOF I TAXIED INTO POS AND AN OIL LIGHT CAME ON FOR THE L ENG. WE INFORMED TWR AND WERE INSTRUCTED TO TAXI TO THE INTXN AND CONTACT GND. WE TAXIED TO THE GATE AND I SHUT DOWN #1 AND LEFT #2 RUNNING UNTIL PWR WAS ON (GPU). THE MECHS HAD THE COWL OPEN AND HAD INFORMED ME THAT THEY HAD LEFT THE OIL CAP OFF AND AS SOON AS THEY GOT THE ENG FILLED BACK UP WE WOULD BE ON OUR WAY. THE INCIDENT WAS NOT PUT IN THE MAINT LOG BECAUSE I FELT THAT; 1) NOTHING WAS BROKEN; AND 2) NOTHING WAS FIXED. THE TIMES ENTERED INTO THE ACFT LOG REFLECTED ONLY THE SECOND DEP FROM THE GATE DUE TO A MISUNDERSTANDING OF WHAT SHOULD BE ENTERED ON THE FLT LOG AND WHAT SHOULD BE ENTERED ON THE PAYROLL FORM. I BELIEVE THAT OUR PRINCIPLE OPS INSPECTOR (POI) THINKS THAT I INTENTIONALLY COVERED UP THE INCIDENT; WHICH I HAVE NOT. I MADE A MISTAKE ON THE FLT LOG DUE TO BEING TIRED AND RUSHED; AND I MADE A JUDGEMENT CALL THAT IS BEING QUESTIONED. I THOUGHT ABOUT MY DECISION ON THE WAY HOME TODAY AND CONCLUDED THAT ANYTIME YOU ALTER YOUR PLAN OF FLT DUE TO ANY INDICATION OF EQUIP MALFUNCTION IT IS BEST TO WRITE UP THE INCIDENT WHETHER IT SEEMS APPROPRIATE OR NOT. AND WHEN YOU ARE TIRED AND LATE; TAKE SOME TIME OUT TO MAKE SURE YOU ARE NOT SKIPPING SOMETHING IMPORTANT.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.