AN AIRBUS 320 ON RUN AFTER MAINT OVERTEMPED #2 ENG DUE TO FAILURE TO CONNECT THE COMPRESSOR STATOR VANE ACTUATOR.

Date: 2000-01 · Aircraft: A320 · Phase: ground

Anomalies: aircraft-equipment-problem-critical|deviation-discrepancy-procedural-maintenance|deviation-discrepancy-procedural-published-material-policy

Synopsis

AN AIRBUS 320 ON RUN AFTER MAINT OVERTEMPED #2 ENG DUE TO FAILURE TO CONNECT THE COMPRESSOR STATOR VANE ACTUATOR.

Narrative

ON JAN/XA/00; ANOTHER MECH AND MYSELF WERE ASSIGNED TO WORK THE R SIDE OF ENG #2 ON AN AIRBUS A320/V2500 ENG. WE WERE TO REPLACE THE UPPER AND LOWER THIRD STAGE VARIABLE STATOR VANE ARMS. PART OF THE PREPARATION WORK INVOLVED DISCONNECTING THE VARIABLE STATOR VANE ACTUATOR ROD END FROM THE SEGMENT RING; IN ORDER TO INSTALL A RIG PIN. THIS INSURES PROPER RIGGING. IT'S MAINTAINED WHILE THE ARMS ARE BEING REPLACED. UPON COMPLETION OF JOB; THE LAST THING THE CHANGE ORDER AUTH INSTRUCTS YOU TO DO IS TO REMOVE THIS RIG PIN AND RECONNECT THE ROD END TO THE SEGMENT RING. AN ACFT INSPECTOR IS THEN CALLED TO INSPECT THE ENTIRE REPAIR FOR SAFETY AND SECURITY. A LINE MECH DOES AN OPS CHK OF ENG AFTER THE INSPECTOR SAYS IT'S OK. THE OTHER MECH AND MYSELF WORKED THE LATE NIGHT SHIFT. AT THE END OF OUR SHIFT; WE HAD COMPLETED THE REMOVAL AND INSTALLATION OF ALL 8 VARIABLE STATOR VANE ARMS. WE DID NOT HAVE THE TIME TO REINSTALL THE PARTS REMOVED FOR ACCESS. THESE PARTS INCLUDED THE UNISON RING; WHICH CONNECTS THE UPPER TO THE LOWER SEGMENT. THE RIG PIN WAS LEFT IN PLACE WITH THE ACTUATOR ROD END DISCONNECTED. ALL REMOVED PARTS WERE TAGGED AND LABELED AND LAID OUT ON A WORK TABLE NEXT TO THE ENG. I STATED ON THE FRONT OF THE SIGN-OFF DOCUMENT WHAT WE HAD ACCOMPLISHED. I ALSO GAVE A STATUS RPT TO OUR TEAM LEADER; WHICH IS THEN PASSED ON TO THE DAY SHIFT TEAM LEADER. THE DAY SHIFT THEN BRIEFS THE MECH WHO WILL BE TAKING OVER THE JOB AS TO WHAT NEEDS TO BE DONE TO COMPLETE THE JOB. A DAY SHIFT MECH TOOK OVER FROM WHERE WE LEFT OFF. HE COMPLETED THE INSTALLATION; REMOVED THE RIG PIN; BUT FAILED TO RECONNECT THE ACTUATOR ROD END BACK TO THE SEGMENT RING. THE DAY SHIFT ACFT INSPECTOR THEN INSPECTED THE COMPLETED INSTALLATION. THIS INSPECTOR ALSO FAILED TO MAKE SURE THAT THE MECH HAD ATTACHED THE ROD END BACK TO THE SEGMENT RING. HE OK'ED THE ENTIRE JOB AS BEING COMPLETED. A LINE MECH THEN TEST RAN THE ENG; WHICH RESULTED IN AN OVERTEMPING OF THE ENG. THIS ENG WAS THEN REMOVED FROM THE ACFT AND REPLACED WITH A SPARE.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.