A B757-200 FLC EVACS A FULLY LOADED ACFT AFTER MAKING A DIVERSION AND AN EMER LNDG DUE TO TOXIC FUMES IN THE COCKPIT AND CABIN 40 MI N OF BNA; TN.
Synopsis
A B757-200 FLC EVACS A FULLY LOADED ACFT AFTER MAKING A DIVERSION AND AN EMER LNDG DUE TO TOXIC FUMES IN THE COCKPIT AND CABIN 40 MI N OF BNA; TN.
Narrative
AT APPROX XA00Z AT FL330 AND 40 NM N OF BNA; WE HAD A FOUL NOXIOUS ODOR IN THE COCKPIT. CHKING WITH THE FIRST CLASS FLT ATTENDANTS; WE FOUND THAT THEY ALSO HAD A BURNING SULFUR-LIKE ODOR IN THE CABIN. THEY QUICKLY CHKED TO BE SURE THAT THE ODOR WAS NOT COMING FROM THE OVENS OR FROM SOMEONE SMOKING IN THE LAVATORIES. THE ODOR WAS OVERPWRING; SO THE DECISION WAS MADE TO DIVERT INTO BNA. ATC WAS NOTIFIED. FO FLEW THE AIRPLANE WHILE I RAN THE CHKLISTS. THE TIME FROM THE FIRST SMELL TO TOUCHDOWN WAS APPROX 12 MINS. WHILE IN THE DSCNT; I INFORMED THE FLT ATTENDANTS THAT WE MIGHT NEED TO DO AN EMER EVAC AND TO PREPARE THE CABIN. AFTER LNDG; I WAITED TO SEE IF THE SMELL WOULD DISSIPATE. AFTER ABOUT 1 MIN THE SMELL WAS GETTING STRONGER -- I GAVE THE ORDER TO EVAC. OUR FLT ATTENDANTS DID AN OUTSTANDING JOB. I TALKED WITH THE PAX AT THE EMER WING EXITS AND THEY WERE BRIEFED AND UNDERSTOOD WHAT THEY HAD TO DO PERFECTLY. THE ACFT WAS EVACED IN EXCELLENT TIME; WITH ONLY MINOR INJURIES. OUR FLT ATTENDANTS WERE CALM; PROFESSIONAL AND COMPLETELY IN CHARGE OF THE SIT. ONCE THE PAX WERE OFF THE ACFT; THEY WERE MOVED TO A SAFE DISTANCE AND THE FLT ATTENDANTS STARTED EVALUATING AND HELPING THOSE WHO HAD MINOR SCRAPES AND BRUISES. SUPPLEMENTAL INFO FROM ACN 513068: THE ACFT WAS EVACED RAPIDLY WITH ONLY MINOR INJURIES TO LESS THAN A DOZEN PAX. THE PAX WERE GROUPED TOGETHER OFF THE RWY ON EITHER SIDE OF THE ACFT. WE TOOK THE NAMES OF THE INJURED AND DIRECTED THEM TO THE EMT'S; WHILE WE TRIED TO CALM THE REST OF THE PAX. BUSSES CAME TO BRING THE PAX TO THE TERMINAL ABOUT 1 HR AFTER WE TOUCHED DOWN. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: FO RPTR SAID THAT HE LATER FOUND OUT THAT THE FUMES CAME FROM AN OVERHEATED WIRE BUNDLE THAT SUPPLIED CURRENT TO THE L2 COCKPIT WINDOW FOR INFLT HEATING. APPARENTLY THE CIRCUIT BREAKERS HAD NOT OPENED TO CUT THE ELECTRICAL FROM THE ERRANT PWR SOURCE. HE ALSO STATED THAT WHEN HE ENTERED THE CABIN DURING THE EVAC ON THE GND; PAX WERE ALL LINED UP IN ROWS WAITING TO USE THE PORT SIDE EXITS WHILE THE STARBOARD EXITS WERE COMPLETELY FREE. HE DIRECTED PAX TO USE THOSE EXITS AS WELL. THE ACFT HAD BEEN CARRYING A FULL LOAD OF PAX. SOME PAX HURT THEIR FINGERS WHEN THEIR RINGS WOULD CATCH ON A HINGE OR A PART OF THE ACFT. OTHERS HURT THEMSELVES AT THE BOTTOM OF THE CHUTE DUE TO A HIGHER THAN EXPECTED DSCNT RATE. THIS IS CAUSED BY THE EXTRA TALL LNDG GEAR ON THE B757; MAKING IT A PROB FOR PAX TO KEEP THEIR BAL ON THE LAST PART OF THEIR RIDE. THIS SHOWS THE NEED FOR MONITORS AT THE BOTTOM OF THE CHUTE TO ASSIST THE PAX.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.