AN AIRBUS RETURNED TO THE FIELD DUE TO FORWARD CARGO DOOR FAILURE. SEAL FOUND IMPROPERLY INSTALLED WITH INFLATION HOLES BLOCKED WITH SEALANT.
Synopsis
AN AIRBUS RETURNED TO THE FIELD DUE TO FORWARD CARGO DOOR FAILURE. SEAL FOUND IMPROPERLY INSTALLED WITH INFLATION HOLES BLOCKED WITH SEALANT.
Narrative
WHEN I CHANGED THE SEAL; I FIRMLY BELIEVED I READ IN AMM 52-31-18 TO FILL ALL THE HOLES WITH RTV (ELASTIC SEALANT). I THOUGHT AT THE TIME IT WAS ODD; BUT DID IT THE WAY I THOUGHT I HAD READ IT. I EVEN MENTIONED IT TO MY LEAD WHO SAID; IF THAT'S WHAT THE MANUAL TELLS YOU TO DO IT. LOOKING AT A CURRENT AMM REF; I DO NOT SEE ANYTHING TELLING ME TO FILL ALL THE HOLES ON THE SEAL. I BELIEVE I MUST HAVE MISREAD THAT PORTION. I BELIEVE HUMAN FACTORS PLAYED A MAJOR PART IN THIS INCIDENT AS I AM UNDER A TREMENDOUS AMOUNT OF PRESSURE AND STRESS. SINCE I LEFT OFFICE MGMNT (PARTICULARLY DIRECTOR MR X) AND A FEW EMPLOYEES HAVE ATTEMPTED TO SET ME UP FOR TERMINATION; INCLUDING POSSIBLE SABOTAGE. I HAVE FILED GRIEVANCES (PENDING ARBITRATION) AND HARASSMENT EEO COMPLAINTS; WITHOUT RESULT. MY FELLOW CREW MEMBERS EVEN FEEL THE STRESS FROM THIS EXTREMELY HOSTILE WORK ENVIRONMENT. I AM SURPRISED I HAVEN'T MADE A MISTAKE BEFORE THIS. THIS IS THE 1ST INCIDENT I HAVE BEEN INVOLVED IN DURING MY 17+ YRS AT ACR X. I BELIEVE THIS HOSTILE ENVIRONMENT MUST BE STOPPED BEFORE WE ARE INVESTIGATING A MAJOR INCIDENT.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.