DISPATCHER RELIEVED OF DUTY AFTER A B727 FLT CONTINUATION WHEN FLT CREW ONLY COORDINATED WITH MAINT CTLR ON THE 'LOW OIL PRESSURE LIGHT-FILTER BYPASS LIGHT ILLUMINATED' WITH FLT OPERATING TO DEST ARPT; ON FREQ WITH ZZZ. US.

Date: 2004-07 · Aircraft: B727 Undifferentiated or Other Model · Phase: cruise

Anomalies: aircraft-equipment-problem-critical|deviation-discrepancy-procedural-maintenance|deviation-discrepancy-procedural-other-unknown|deviation-discrepancy-procedural-published-material-policy|deviation-discrepancy-procedural-mel-cdl|other-flight-crew-dispatch-relationship

Synopsis

DISPATCHER RELIEVED OF DUTY AFTER A B727 FLT CONTINUATION WHEN FLT CREW ONLY COORDINATED WITH MAINT CTLR ON THE 'LOW OIL PRESSURE LIGHT-FILTER BYPASS LIGHT ILLUMINATED' WITH FLT OPERATING TO DEST ARPT; ON FREQ WITH ZZZ. US.

Narrative

CREW CONTACTED DISPATCH VIA NY CTL. FLT HAD DEPARTED DFW AND HAD REFERENCED THEIR 'COCKPIT OPS MANUAL'; THAT INVOLVED THE LOW OIL PRESSURE OR FILTER BYPASS LIGHT ILLUMINATED. I CONFIRMED WITH THEM TO PROCEED OR SPEAK WITH MAINT CTL. THE OIL PRESSURE WAS IN THE GREEN BAND AND TEMPS WERE NORMAL. THE MAINT CTLR ADVISED THE CREW TO CONTINUE TO PVR AND MAINT WOULD MED THEM ON ARR THE MANUAL STATES THAT: 'ACCOMPLISH THE ENGINE PRECAUTIONARY SHUTDOWN PROC IN THE SECTION; OR; IF NECESSARY; OPERATE THE ENGINE AT THE MINIMUM THRUST REQUIRED FOR SAFE COMPLETION OF FLT.' THE MAINT CTLR TERMINATED THE PHONE PATCH. I VERIFIED WITH MAINT CTL THAT THE CREW WAS COMFORTABLE WITH CONTINUING ON AND WITH THE DECISION. HE SAID 'YES.' UPON ARR IN PVR; MAINT CTL MEL'ED THE 'LOW OIL PRESSURE LIGHT' UNDER THE ASSUMPTION THE SWITCH WAS THE ISSUE. AFTER RETURNING TO DFW; MAINT RAN THE ENGINE AND THE LIGHT DID NOT ILLUMINATE. SEVERAL HRS LATER MAINT RAN THE ENG AGAIN AND STILL NO LIGHT ILLUMINATED; THE MEL WAS CLRED. TWO DAYS LATER THE FLT (SAME ACFT) DEPARTED AND ON CLBOUT THE LIGHT ILLUMINATED. A PHONE PATCH WAS INITIATED WITH DISPATCH AND MAINT CTL. MAINT CTL ADVISED THE CREW TO RETURN TO ORIGINATION CITY. IT WAS LATER FOUND THAT THERE WAS METAL IN THE BYPASS. I WAS REMOVED FROM DISPATCH AUTH TO A FLT FOLLOWING POS UNTIL AN INTERNAL INVESTIGATION WAS COMPLETED FOR NOT UPHOLDING 'OPERATIONAL CTL.' I SHOULD HAVE RE-ESTABLISHED COM WITH THE CREW TO CONFIRM THEY WERE COMFORTABLE WITH THE DECISION.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.