B757-200 CAPT RPTS WINDSHEAR ENCOUNTER IN DEN. DIVERT TO COS.

Date: 2005-07 · Aircraft: B757-200

Anomalies: deviation-speed-all-types|inflight-event-encounter-weather-turbulence|inflight-event-encounter-other-unknown

Synopsis

B757-200 CAPT RPTS WINDSHEAR ENCOUNTER IN DEN. DIVERT TO COS.

Narrative

PREVIOUS DAY JUL/FRI/05 WAS OVER 12 HR DUTY DAY AND 7 HRS 48 MINS OF FLT TIME; CREEPING MECHANICAL IN DENVER. GOT TO CYVR 3 HRS LATE. DELAYED DEP NEXT DAY TO GET MINIMUM REST AT HOTEL. WENT ON DUTY AT XA00. TRIED TO LEAVE CYVR BUT EXPERIENCED SAME HYD PROB AS PREVIOUS DAY AND RETURNED TO GATE AFTER 30 MIN TAXI. SPENT THE NEXT 7 HRS WORKING WITH MECHS TO TRY TO FIX PROB. MINIMAL FOOD; NO REST. RAN UP ENGS ONCE. STAYED ON THE AIRPLANE OUT ON A HARD STAND ALL DAY. WAS ASKED TO FERRY ACFT TO DENVER. TOOK ANOTHER 2 HRS TO GET APPROPRIATE PAPERWORK AND FUEL TO DEPART. FLT TO DEN WAS FINE; HOWEVER; BY THE TIME OF ARR; WAS PAINTING A STORM N OF THE FIELD. WAS VECTORED TO FINAL FOR RWY 35L. DISCUSSED WINDSHEAR PRECAUTIONS AND ADDED 20 KTS TO REF. NO WINDSHEAR RPTED BY TWR. AFTER THE 500 FT CALL; GOT A WINDSHEAR WARNING (SAME TIME TWR CALLED A MICROBURST ALERT) AND INITIATED A GAR. WINDSHEAR WAS SEVERE. RPTED IT TO TWR AND WAS GIVEN GAR INSTRUCTIONS. COULD BARELY READ INSTS; WAS ATTEMPTING TO TURN R TO A HDG OF 120 DEGS WHEN TWR ASKED US TO EXPEDITE TURN FOR TFC. I TOLD THEM THAT WE WERE IN SEVERE WINDSHEAR AND 'DOING THE BEST THAT WE CAN.' DURING CLEANUP OF FLAPS; GOT A MOMENTARY FLAP LIMIT ANNUNCIATION WHEN FLAPS WERE TRANSITIONING BTWN 1 DEG AND 0 DEGS; SPD 240 KTS. RECOVERED FROM THE WINDSHEAR AND LEVELED OFF. WX WAS NOT LOOKING GOOD AT PUEBLO; EVERYONE BEHIND US AT DEN WAS GOING AROUND; SO WE REQUESTED A DIVERT TO COS. WE HAD ALREADY AGREED PRIOR TO THE APCH THAT IN THE EVENT OF A GAR FOR ANY REASON THAT WE WOULD DIVERT AND STOP FOR THE DAY. SO; AT THIS POINT THERE WAS NOT MUCH MORE DISCUSSION OTHER THAN WHERE TO GO. SENT MESSAGE TO DISPATCH; CALLED COS. INFORMED DUTY FLT MGR BY PHONE AFTER LNDG. FO AND I BOTH AGREED THAT WE WERE DONE FLYING FOR THE DAY AND ASKED TO BE RELEASED FROM DUTY. FO DID AN EXCELLENT JOB DURING THE WINDSHEAR RECOVERY AND SUBSEQUENT DIVERSION. HUMAN FACTORS: WE ARE NOW SO FATIGUED AFTER 2 DAYS OF THIS THAT THERE IS NO WAY THAT WE COULD FUEL THE AIRPLANE AND SAFELY ATTEMPT TO FLY EVEN 15 MINS TO DEN. EXTREMELY FORTUNATE THAT THIS ACFT WAS EMPTY; WAS A LIGHT LNDG WT AND THAT WE HAD BRIEFED AND THEN PROPERLY EXECUTED WINDSHEAR RECOVERY. SUCCESSFUL OUTCOME AND LNDG AT COS.

More incidents for this aircraft family →

Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.