A NEW CRJ200 CAPT AND LOW TIME FO WERE GIVEN A CLOSE-IN RWY CHANGE TO ATL. AFTER LNDG THE CAPT NARROWLY MISSED A RWY INCURSION.
Synopsis
A NEW CRJ200 CAPT AND LOW TIME FO WERE GIVEN A CLOSE-IN RWY CHANGE TO ATL. AFTER LNDG THE CAPT NARROWLY MISSED A RWY INCURSION.
Narrative
WE WERE ON THE HONIE FIVE RNAV ARR INTO ATL. WE WERE NOTIFIED BY APCH CTL TO EXPECT RWY 28. WE THEN THOROUGHLY BRIEFED THE APCH AND THE TAXI-IN PROC FROM RWY 28 TO RAMP. A FEW MILES PRIOR TO WOLMN; APCH CTL TOLD US TO NOW EXPECT RWY 26R. WE WERE ALSO TOLD TO FLY DIRECT TO FANEW; EXPEDITE OUR DSCNT TO 2000 FT AND EXPECT A SHORT APCH. AS WE WERE DSNDING; I TOLD THE FO TO BRIEF THE NEW APCH PROC. BASE TURN CAME RATHER RAPIDLY AND VERY LITTLE TIME WAS ALLOCATED TO REVIEW THE TAXI-IN PROC FROM RWY 26R TO RAMP. AFTER LNDG; WE CLEARED THE RWY ON B3 AND WERE TOLD BY TOWER CTL TO 'JOIN TXWY VICTOR AND CONTACT GND ON 121.9.' GND THEN TOLD US TO TAXI TO OUR GATE. AS WE APCHED THE VICTOR/HOTEL INTXN; I MISTAKENLY FOLLOWED THE HOTEL TAXI-LANE AS OPPOSED TO THE VICTOR TAXI-LANE. MY ERROR WAS PARTLY DUE TO THE MISINTERPRETATION OF THE VICTOR DIRECTION SIGN AND THE SHALLOW ANGLE BETWEEN THE VICTOR AND HOTEL TAXI-LANE AT THAT PARTICULAR LOCATION. AS I TURNED ONTO HOTEL; I SAW THE HOLD SHORT LINE FOR THE DEP END OF RWY 26L AND STOPPED. I QUERIED GND CTL WHETHER WE WERE CLEARED TO CROSS RWY 26L/8R. GND TOLD US THAT WE TURNED ON THE WRONG TXWY AND THEN ASKED US TO REJOIN VICTOR; WHICH WE DID. THE REST OF THE FLT WAS UNEVENTFUL. FACTORS: 1) BRAND NEW CAPT; SECOND TRIP AFTER OE. 2) BRAND NEW FO; FIRST TRIP AFTER OE. 3) UNFAMILIAR ARPT. 4) LAST MINUTE CLRNC CHANGE; AND LACK OF TIME ALLOCATED TO BRIEF ANTICIPATED TAXI-IN PROC. 5) RUSHED TOWARDS THE END OF THE ARR PROC AND TAXI. SUGGESTIONS: 1) REVIEW MORE THAN ONE TAXI-IN POSSIBILITIES; FROM MORE THAN ONE RWY ASSIGNMENT ON THE APCH BRIEF. 2) DO NOT ALLOW THE FO TO DO ANYTHING BUT KEEP HIS EYES OUTSIDE WHILE TAXIING ON AN UNFAMILIAR ARPT. DELAY CHECKLISTS. POSITIVE ELEMENTS OF THIS INCIDENT. WHEN UNSURE OF OUR POSITION; WE STOPPED AND QUERIED ATC. WE WERE THANKED BY ATC FOR THAT.CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THAT THIS WAS HIS SECOND TRIP OFF OF IOE AND THE FO'S FIRST TRIP OFF OF NEW HIRE IOE AND HIS FIRST TRIP TO ATL. THE RPTR FELT AS IF HE WAS IN A SINGLE PLT OPERATION. THE LATE RWY CHANGE DID NOT ALLOW HIM ENOUGH TIME TO GET HIS RWY 26R APCH PLATE OUT OF HIS APCH PLATE BOOK. AFTER LNDG THE FO WAS DOING HIS AFTER LNDG FLOW AND THEREFORE WAS HEADS DOWN IN THE COCKPIT. THE RPTR STATED THAT WHEN HE CAME UP TO TXWY H AND SAW THE HOLD SHORT LINE; HE REALIZED SOMETHING WAS NOT CORRECT. HE HAD ENOUGH ROOM TO TURN AROUND AT THAT POINT AND CORRECT HIS MISTAKE. ATC ASKED HIM TO CALL AT THE GATE AND THANKED HIM FOR STOPPING WHEN HE WAS UNCERTAIN ABOUT WHERE HE WAS. THE RPTR EXPLAINED TO ATC THE SCENARIO LEADING UP TO THIS EVENT AND RELAYED TO THEM THAT THE CREW HAD BEEN RUSHED INTO ACCEPTING A RWY CHANGE AT THE LAST MINUTE. ATC'S RESPONSE WAS THAT CREWS MUST BE READY FOR ANYTHING.
More incidents for this aircraft family →
Source: NASA Aviation Safety Reporting System (public domain). Reports are voluntary submissions and are not verified by NASA.