Engine Retraction Malfunction Leads to Forced Landing in Pipistrel Taurus 503

Casualties unknown • Stary Wielisław, koło Polanicy-Zdroju, PL

An ultralight aircraft experienced a mechanical failure during engine retraction, resulting in an undershoot and landing on an agricultural field near Stary Wielisław.

What happened

On September 14, 2019, a pilot and the aircraft owner departed from a landing strip in Stary Wielisław for a local flight. While flying at approximately 1,000 meters in the Bystrzyca Kłodzka region, the pilot attempted to shut down the engine to utilize thermal updrafts for gliding.

Following the deactivation of the magnetos, the engine seized while the propeller remained in motion. The pilot reported hearing an unusual noise but determined the Pipistrel Taurus 503, registration SP-STAU, remained fully controllable. The pilot decided to return to the departure airfield; however, the aircraft experienced a higher-than-normal rate of descent due to the non-functioning, protruding engine assembly.

As the pilot transitioned to a landing approach on runway 33, they realized the aircraft was too low to reach the landing strip. The aircraft subsequently landed short of the runway on a plowed field. During the landing roll on the uneven terrain, the wingtips struck the ground several times before the aircraft came to a stop approximately 30 meters from the runway threshold. There were no injuries reported.

The investigation

The PKBWL examined the mechanical sequence of the engine retraction system. The standard automated procedure requires the engine to shut down, the propeller to come to a complete stop, and the propeller to reach a vertical position before the engine and propeller assembly retract into the fuselage.

The investigation established that an incorrect and incomplete retraction sequence occurred, which caused the control mechanism to jam. This malfunction resulted in damage to the engine cowlings and the propeller edge. While the pilot suggested a momentary sensor failure might have caused the malfunction, a manufacturer inspection found no issues with the mechanical actuator or the sensor. Following repairs, the aircraft was returned to service.

Findings

  • The primary cause of the incident was a momentary malfunction of the control system responsible for the engine retraction mechanism.
  • The improper retraction sequence led to the engine assembly becoming stuck in a protruding position.
  • The landing on uneven, plowed terrain caused additional damage to the landing gear and wingtips.

Probable cause

A temporary failure in the control system for the engine retraction mechanism prevented the propeller from reaching the required vertical position before retraction was initiated, leading to a jammed mechanism and an unstable glide.

Frequently asked questions

What happened in the 2019-09-14 PIPISTREL, Taurus 503 accident near Stary Wielisław, koło Polanicy-Zdroju, PL?

An ultralight aircraft experienced a mechanical failure during engine retraction, resulting in an undershoot and landing on an agricultural field near Stary Wielisław.

What aircraft was involved and where did it happen?

The accident on 2019-09-14 involved a PIPISTREL, Taurus 503, registration SP-STAU, operated by Pilot samolotu ultralekkiego, at Stary Wielisław, koło Polanicy-Zdroju, PL.

What was the probable cause of the accident?

A temporary failure in the control system for the engine retraction mechanism prevented the propeller from reaching the required vertical position before retraction was initiated, leading to a jammed mechanism and an unstable glide.

Investigation report by the Polish State Commission on Aircraft Accidents Investigation (PKBWL). Original record: https://pkbwl.gov.pl/raporty/2019-4172/. This page is a structured re-presentation; facts and quotes are in the Panstwowa Komisja Badania Wypadkow Lotniczych (PKBWL), Poland.

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