Engine Failure Leads to Runway Excursion in Cessna 152 Training Flight

Casualties unknown • GUARAPARI, ES, BR

A training flight in Guarapari, Brazil, resulted in substantial aircraft damage after a spark plug detachment caused engine power loss and a runway excursion.

What happened

On December 28, 2016, a Cessna 152, registration PR-KNE, was performing a local instructional flight at the Guarapari Aerodrome (SNGA) in Espírito Santo, Brazil. The aircraft was occupied by a flight instructor and a student pilot. During the return leg of the flight, approximately 4 nautical miles from the airfield, the crew experienced intense engine vibration and abnormal noise, followed by a significant loss of engine power.

The instructor took control of the aircraft to perform an emergency landing. The aircraft touched down on the final third of the runway; however, due to the remaining runway length, the aircraft could not come to a complete stop within the paved limits, resulting in a runway excursion. The impact caused substantial damage to the nose gear, engine mount, lower engine cowling, right wing, and rudder. Both occupants were uninjured.

The investigation

CENIPA investigators examined the Lycoming 0-235-L2C engine and identified that the lower spark plug of cylinder number one had detached. Laboratory analysis conducted by the Department of Aerospace Science and Technology (DCTA) revealed that the failure was caused by wear in the cylinder's female thread, which led to the subsequent detachment of the helicoil along with the spark plug.

The investigation noted that the aircraft had undergone a 100-hour inspection just seven days prior to the accident. According to the Lycoming Operator’s Manual, such inspections require the removal, testing, and cleaning of spark plugs. The investigation determined that the failure to identify the thread wear during this recent maintenance period indicated that the inspection services were not performed adequately.

Findings

  • Inadequate maintenance: The failure to detect the worn cylinder threads during the 100-hour inspection was a contributing factor.
  • Management oversight: Deficiencies in the technical supervision of maintenance activities within the organization contributed to the occurrence.
  • Pilot judgment: The decision-making regarding the emergency landing parameters contributed to the aircraft exceeding the runway limits.

Safety action

CENIPA issued a safety recommendation to the National Civil Aviation Agency (ANAC) to work with the operator to ensure that 50-hour and 100-hour inspections for Lycoming O-235 and O-290 series engines strictly adhere to the manufacturer's manual and regulatory requirements regarding the removal, analysis, and installation of spark plugs.

Probable cause

The engine failure was caused by the detachment of a spark plug due to worn cylinder threads, which went undetected during a recent 100-hour inspection. The accident was further compounded by inadequate maintenance execution, lack of technical supervision, and improper pilot judgment during the emergency landing.

Frequently asked questions

What happened in the 2016-12-28 aircraft accident near GUARAPARI, ES, BR?

A training flight in Guarapari, Brazil, resulted in substantial aircraft damage after a spark plug detachment caused engine power loss and a runway excursion.

What aircraft was involved and where did it happen?

The accident on 2016-12-28 involved a aircraft, registration PRKNE, at GUARAPARI, ES, BR.

What was the probable cause of the accident?

The engine failure was caused by the detachment of a spark plug due to worn cylinder threads, which went undetected during a recent 100-hour inspection. The accident was further compounded by inadequate maintenance execution, lack of technical supervision, and improper pilot judgment during the emergency landing.

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