Nose gear collapse during landing at Otherton Airfield

Casualties unknown • Otherton Airfield, Staffordshire, GB

A Mercury microlight sustained significant damage after its nose gear collapsed during a landing on a grass runway in Staffordshire.

What happened

On 2 July 2017, a Mercury microlight, registration G-MYUB, was performing a private flight when it experienced a landing accident at Otherton Airfield, Staffordshire. During the landing sequence on grass Runway 34, the pilot successfully touched down on the main wheels. However, shortly after the initial contact, the nosewheel made contact with the ground. Upon this contact, the nose gear failed, causing the aircraft to tip onto its left side. The aircraft slid approximately 10 feet before coming to a complete stop.

There were two people on board at the time of the accident. The passenger escaped without injury, while the pilot sustained minor injuries. The aircraft itself incurred substantial damage, specifically affecting the propeller, the wing, the nose gear, and the pod/trike unit.

The investigation

Following the incident, the AAIB examined the wreckage and the circumstances of the landing. A subsequent inspection conducted by an independent third-party organisation focused on the structural integrity of the landing gear. This technical examination revealed a fatigue crack located at the edge of a weld on the nose gear assembly. It was determined that this crack caused the component to fail when subjected to the loads experienced during the landing touchdown.

Probable cause

The nose gear collapsed due to a fatigue crack at the edge of a weld, which failed under the load of the landing.

Frequently asked questions

What happened in the 2017-07-02 Mercury accident near Otherton Airfield, Staffordshire, GB?

A Mercury microlight sustained significant damage after its nose gear collapsed during a landing on a grass runway in Staffordshire.

What aircraft was involved and where did it happen?

The accident on 2017-07-02 involved a Mercury, registration G-MYUB , at Otherton Airfield, Staffordshire, GB.

What was the probable cause of the accident?

The nose gear collapsed due to a fatigue crack at the edge of a weld, which failed under the load of the landing.

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