Loss of control during landing leads to microlight crash on Lundy Island

Casualties unknown • Lundy Island Airfield, Bristol Channel, GB

A Quik GT450 microlight sustained extensive damage after a mechanical failure caused severe pitch control difficulties during its approach to Lundy Island.

What happened

On 17 May 2023, a Quik GT450 microlight, registration G-CEVW, was performing a private flight from Lundy Island back to Park Hall Farm Airfield. Shortly after departing Lundy Island at 1215 hrs, the pilot experienced a sudden and significant pitch-up tendency accompanied by a reduction in airspeed. The pilot found the control forces to be extremely heavy, noting that he had to wedge the control bar under his arms to maintain control of the aircraft.

Unable to maintain a stable flight path, the pilot decided to return to Lundy Island. During the approach to runway 24, the aircraft's response remained sluggish and the control loads remained extreme. The pilot attempted to manage the approach despite being poorly aligned with the runway, fearing that a go-around would be impossible due to the physical strength required to manipulate the controls. The aircraft made a heavy touchdown, resulting in extensive damage to the wing and airframe, and the collapse of the nose landing gear. The pilot sustained minor injuries and was able to exit the aircraft without assistance.

The investigation

The AAIB examined the wreckage at a storage facility and found that the wing structure had been severely deformed and the sail material ripped. Investigation of the wing keel revealed that the roll bearing had migrated approximately 300 mm rearward along the keel tube. This movement had caused the bearing to strike the trim attachment bracket, leaving visible witness marks.

The investigators determined that the M6 caphead bolt and its associated Nylok nut, which were responsible for securing the roll bearing in place, were missing. The loss of this single bolt allowed the hang bracket and roll bearing to slide aft, which shifted the aircraft's center of gravity and induced the severe nose-up pitch that the pilot encountered.

Probable cause

The loss of the roll bearing securing bolt caused the hang bracket to move rearward along the wing keel, inducing a significant pitch-up tendency and extreme control loads that made the aircraft difficult to fly.

Frequently asked questions

What happened in the 2023-05-17 Quik GT450 accident near Lundy Island Airfield, Bristol Channel, GB?

A Quik GT450 microlight sustained extensive damage after a mechanical failure caused severe pitch control difficulties during its approach to Lundy Island.

What aircraft was involved and where did it happen?

The accident on 2023-05-17 involved a Quik GT450, registration G-CEVW, at Lundy Island Airfield, Bristol Channel, GB.

What was the probable cause of the accident?

The loss of the roll bearing securing bolt caused the hang bracket to move rearward along the wing keel, inducing a significant pitch-up tendency and extreme control loads that made the aircraft difficult to fly.

Loading the flight search…