Engine Failure Leads to River Ditching of Beechcraft A36 near Fukui

Casualties unknown • Northwest of Fukui Airport, JP

A privately owned Beechcraft A36 experienced continuous engine power loss, forcing the pilot to perform a ditching in a river northwest of Fukui Airport.

What happened

On October 15, 2017, at approximately 15:36 JST, a privately owned Beechcraft A3-6, registered JA3842, was conducting a flight approach to Fukui Airport when the engine began to lose power. The aircraft was flying at an altitude of roughly 300 meters, approximately four kilometers northwest of the airfield. During the approach to the traffic pattern, a passenger noticed engine abnormalities, and the pilot attempted to stabilize the engine by adjusting the fuel selector valve from the right tank to the left tank. However, the power loss persisted.

Unable to reach the runway, the pilot performed several maneuvers, including adjustments to the propeller, mixture, and starter switch, while searching for a suitable landing site. The pilot ultimately decided to perform a forced landing and ditched the aircraft in a nearby river. Following the impact, all occupants successfully evacuated the submerged aircraft and swam to the riverbank. The aircraft sustained minor damage, including a deformed nose landing gear door and a detached right main gear.

The investigation

The Japan Transport Safety Board (JTSB) examined the flight history, fuel loading records, and the aircraft's physical condition. Investigators reviewed data from a portable GPS receiver and a vehicle drive recorder installed in the aircraft, which captured cockpit audio and external imagery. The investigation also analyzed the fuel system, specifically the fuel selector valve and the quantities remaining in the tanks after the aircraft was salvaged from the river.

Findings

  • The investigation established that the right fuel tank contained significantly less fuel than the left tank at the time of the incident. While the left tank held approximately 154 liters, the right tank contained only about 1 liter.
  • During a refueling stop at Niigata Airport, the pilot did not visually verify the fuel levels during the preflight inspection, relying instead on fuel quantity indicators.
  • The pilot's awareness of the fuel gauges decreased during the flight due to the need to monitor heavy cloud cover on the route.
  • The engine power loss was caused by the depletion of fuel in the selected right tank, which led to a lack of fuel supply to the engine.
  • The loss of power likely persisted even after the pilot switched the fuel selector to the left tank because air may have entered the fuel system, causing a vapor lock, or the fuel-injected engine may have experienced fuel vaporization due to heat.
  • The engine failure might have been avoided if the pilot had utilized the auxiliary fuel pump as prescribed in the aircraft's emergency procedures.

Probable cause

The engine power loss was caused by the depletion of fuel in the right tank, which the pilot had selected for use. This occurred because the pilot failed to visually confirm fuel levels during preflight and failed to monitor the fuel gauges closely during flight. The continued loss of power after switching tanks was likely due to air entering the fuel system or vapor lock.

Frequently asked questions

What happened in the 2017-10-15 Beachcraft A36 accident near Northwest of Fukui Airport, JP?

A privately owned Beechcraft A36 experienced continuous engine power loss, forcing the pilot to perform a ditching in a river northwest of Fukui Airport.

What aircraft was involved and where did it happen?

The accident on 2017-10-15 involved a Beachcraft A36, registration JA3842, operated by APPROACH, at Northwest of Fukui Airport, JP.

What was the probable cause of the accident?

The engine power loss was caused by the depletion of fuel in the right tank, which the pilot had selected for use. This occurred because the pilot failed to visually confirm fuel levels during preflight and failed to monitor the fuel gauges closely during flight. The continued loss of power after switching tanks was…

Investigation report by the Japan Transport Safety Board (JTSB). Original record: https://jtsb.mlit.go.jp/eng-air_report/JA3842.pdf. This page is a structured re-presentation; facts and quotes are in the Japan Transport Safety Board (JTSB) - Ministry of Land, Infrastructure, Transport and Tourism.

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