AirTran Airways Flight 867 Hydraulic Failure and Runway Excursion

No fatalities • Atlanta-Hartsfield-Jackson, United States of America • Landing (descent or approach)

A Boeing 737-200 experienced a total loss of braking and steering capabilities following an incorrect maintenance repair, leading to a runway excursion at Atlanta International Airport.

What happened

During a postflight inspection at William B. Hartsfield Atlanta International Airport, the first officer of a preceding AirTran Airways flight noticed a leak in the right engine of a Boeing 737-200. Maintenance personnel at the airport identified a chafed hydraulic pressure line related to the right thrust reverser as the source. Following a consultation with a maintenance controller in Orlando, the mechanics were instructed to cap the leaking line and deactivate the right thrust reverser per the airline's Minimum Equipment List.

Instead of capping the intended pressure line, the mechanics incorrectly capped the hydraulic pump case drain return line. A subsequent leak check using the auxiliary power unit and electric pumps failed to reveal the error. The mistake remained undetected until the aircraft entered its climb phase, at which point the overpressurized line caused the hydraulic pump case seal to rupture. This led to the depletion of hydraulic system A fluid.

As the aircraft returned to Atlanta, the crew declared an emergency. The loss of system A fluid disabled several critical components, including the nosewheel steering, ground spoilers, inboard flight spoilers, and both inboard brakes. Although the crew managed to land the aircraft using the rudder, the left thrust reverser, and the outboard brakes, the high landing speed and heavy weight caused the right outboard brake to fail due to friction material depletion. This failure led to a hydraulic leak in system B, subsequently disabling the left outboard brake. Without steering or braking, the aircraft veered off the left side of the runway and ended up in a ditch. There were 0 fatalities.

Findings

  • Maintenance personnel incorrectly identified and capped the hydraulic pump case drain return line instead of the chafed pressure line.
  • The failure to perform an engine-running test prevented the mechanics from detecting the overpressurization of the hydraulic pump.
  • Maintenance staff lacked specific experience with the Boeing 737-200 due to recent company merger transitions.
  • The use of the rudder to maintain directional control during landing depleted the system A accumulator pressure, preventing the use of emergency brake applications.

Probable cause

Incorrect maintenance procedures involving the improper capping of a hydraulic pump case drain line led to a hydraulic system failure during flight.

All Boeing 737-800 accidents →

Frequently asked questions

What happened in the 1998-11-01 Boeing 737-200 accident near Atlanta-Hartsfield-Jackson, United States of America?

A Boeing 737-200 experienced a total loss of braking and steering capabilities following an incorrect maintenance repair, leading to a runway excursion at Atlanta International Airport.

Were there any fatalities in the 1998-11-01 Boeing 737-200 accident?

No fatalities were recorded in this accident.

What aircraft was involved and where did it happen?

The accident on 1998-11-01 involved a Boeing 737-200, registration EI-CJW, operated by AirTran Airways, at Atlanta-Hartsfield-Jackson, United States of America.

What was the probable cause of the accident?

Incorrect maintenance procedures involving the improper capping of a hydraulic pump case drain line led to a hydraulic system failure during flight.

Loading the flight search…