Pressurization Failure Leads to Oxygen Mask Deployment on MD-90 Flight

Casualties unknown • FI

A serious cabin depressurization incident occurred on a Blue1 flight from Helsinki to Oulu when icing in the air conditioning system caused a loss of cabin pressure.

What happened

On 8 January 2007, a Blue1 scheduled flight, KF 201, operating an MD-90-30 from Helsinki to Oulu, experienced a serious pressurization failure while cruising at flight level 350. The incident began when the aircraft's cabin pressure altitude started to rise. The flight crew initially noticed an amber FLOW light, indicating insufficient pressurization capability, as the cabin pressure altitude reached 10,000 feet.

In response, the pilots requested a descent to flight level 210. Shortly thereafter, a red CABIN ALT warning light activated, though it subsequently extinguished due to a malfunction in the pressure sensor. As the cabin pressure altitude continued to climb, reaching 14,000 feet, the passenger oxygen masks deployed. The cabin crew and passengers utilized the masks throughout the descent until the aircraft reached flight level 100. The flight crew also used oxygen masks for portions of the descent. The aircraft eventually completed a normal approach and landing in Oulu.

The investigation

The investigation focused on the failure of the air conditioning and pressurization systems. Investigators examined the state of the air conditioning components and the functionality of the temperature control valves. The probe established that the automatic temperature control for the cabin air conditioning system was inoperative, necessitating the use of manual mode for both the cockpit and cabin systems.

Technical analysis revealed faults in the right temperature control valve, the 35°F water separator control valve, and the cabin altitude warning switch. Furthermore, the investigation looked into the effectiveness of the water separators and the crew's adherence to emergency checklists during the depressurization event.

Probable cause

The primary cause of the incident was the **failure of the 35°F water separator control valve and the temperature control valve**, combined with the use of the air conditioning systems in manual mode, which increased the likelihood of ice accumulation in the water separators. This icing prevented sufficient bleed air from maintaining required cabin pressure.

Frequently asked questions

What happened in the 2007-01-08 aircraft accident near FI?

A serious cabin depressurization incident occurred on a Blue1 flight from Helsinki to Oulu when icing in the air conditioning system caused a loss of cabin pressure.

What aircraft was involved and where did it happen?

The accident on 2007-01-08 involved a aircraft, registration OH-BLU, at FI.

What was the probable cause of the accident?

The primary cause of the incident was the **failure of the 35°F water separator control valve and the temperature control valve**, combined with the use of the air conditioning systems in manual mode, which increased the likelihood of ice accumulation in the water separators. This icing prevented sufficient bleed air…

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