Landing gear retraction incident involving Fournier RF4D at Goodwood

Casualties unknown • Chichester (Goodwood) Airfield, West Sussex, GB

A private flight in a Fournier RF4D experienced an unexpected landing gear retraction shortly after touchdown at Chichester Airfield.

What happened

On 30 January 2010, a Fournier RF4D, registration G-AWEK, was performing a post-restoration check flight at Chichester (Goodwood) Airfield in West Sussex. The aircraft was being operated as a private flight with a single pilot on board.

Shortly after the aircraft had touched down, the landing gear unexpectedly retracted. This caused the aircraft to come to rest on its lower fuselage. There were no injuries to the pilot, and the damage was confined to the nosewheel and the undercarriage.

The investigation

The investigation focused on the mechanical sequence that led to the gear retraction. It was established that the landing gear lever moved out of the DOWN position during the landing roll. The investigation determined that this movement was made possible because a trigger spring allowed the lever to move from its locked position.

Findings

  • The primary cause of the incident was insufficient tension in the landing gear lever trigger spring.
  • This lack of tension allowed the lever to move out of the DOWN position, resulting in the retraction of the landing gear.

Probable cause

The landing gear retracted because insufficient tension in the trigger spring allowed the gear lever to move out of the downward position.

Frequently asked questions

What happened in the 2010-01-30 Fournier RF4D accident near Chichester (Goodwood) Airfield, West Sussex, GB?

A private flight in a Fournier RF4D experienced an unexpected landing gear retraction shortly after touchdown at Chichester Airfield.

What aircraft was involved and where did it happen?

The accident on 2010-01-30 involved a Fournier RF4D, registration G-AWEK, at Chichester (Goodwood) Airfield, West Sussex, GB.

What was the probable cause of the accident?

The landing gear retracted because insufficient tension in the trigger spring allowed the gear lever to move out of the downward position.

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