Engine Failure Leads to Inverted Forced Landing of Van's RV-7A

Casualties unknown • 1,5 km from the threshold of runway 31 at FASY, ZA

A private pilot survived an inverted aircraft rollover after an engine stoppage caused by accidental switch activation during a circuit at Baragwanath aerodrome.

What happened

On 16 July 2013, a Van's RV-7A, registered ZU-FVY, was performing a private flight from Tedderfield aerodrome to Baragontah aerodrome. After completing one touch-and-go on runway 31, the pilot began a right-hand base leg for a second attempt. At an altitude of approximately 500 feet, the engine suddenly ceased operation.

With the engine dead, the pilot initiated an emergency forced landing into an open grass field. Although the pilot attempted to restart the engine by switching fuel tanks and activating the electric pump, the high rate of descent prevented a successful recovery. Upon touchdown, the aircraft's nose gear collapsed due to the rough, uneven terrain, causing the plane to nose over and come to rest in an inverted position. The pilot sustained minor injuries, including lacerations to the head and leg. Because the aircraft was upside down, the canopy could not be slid open; the pilot had to use a portable fire extinguisher to break the plexiglass to escape the wreckage.

Probable cause

The engine stoppage was caused by the simultaneous grounding of both magnetos during flight, likely due to the headset control mechanism making contact with the unguarded switches.

Frequently asked questions

What happened in the 2013-07-16 Van’s RV-7A accident near 1,5 km from the threshold of runway 31 at FASY, ZA?

A private pilot survived an inverted aircraft rollover after an engine stoppage caused by accidental switch activation during a circuit at Baragwanath aerodrome.

What aircraft was involved and where did it happen?

The accident on 2013-07-16 involved a Van’s RV-7A, registration ZU-FVY, at 1,5 km from the threshold of runway 31 at FASY, ZA.

What was the probable cause of the accident?

The engine stoppage was caused by the simultaneous grounding of both magnetos during flight, likely due to the headset control mechanism making contact with the unguarded switches.

Loading the flight search…