What happened
On September 21, 2014, during the "Fly Venice 2014" airshow at the G. Nicelli Airport in Venice Lido, an Xtreme 30/00 aircraft, registration D-EYKS, crashed during an aerobatic performance. The pilot, a highly experienced 57-year-old former aerobatic champion, was performing his second flight of the day.
After takeoff, the aircraft entered a series of aerobatic maneuvers directly above the airfield. During one of these maneuvers, the aircraft entered a descending left-hand spiral. The aircraft struck the ground outside the airport perimeter, impacting a fence and vegetation near a beach facility. The pilot sustained fatal injuries and was found deceased in the cockpit. The aircraft was destroyed upon impact.
The investigation
The ANSV investigation analyzed wreckage, flight logs, and digital data from a FlightDEK-D180 device and a Go-Pro camera. Investigators compared the flight data from the accident to the pilot's successful flight performed earlier that same day.
While the FlightDEK device recorded altitude in feet rather than meters, the investigation established that the pilot initiated the fatal maneuver at a maximum altitude of approximately 1,200 feet (roughly 400 meters). This was significantly lower than the 1,550 feet reached during his successful flight earlier that day.
Video analysis revealed that during the fatal maneuver, the pilot maintained a full back-pressure on the control stick and did not use the rudder to correct the rotation, unlike his previous flight. Evidence suggested the pilot attempted a sudden application of power (a "power burst") to recover the aircraft just before impact, which indicated he remained conscious and aware of the impending collision.
Findings
- The primary cause of the accident was human error, specifically the pilot's inability to recover from the aerobatic maneuver due to insufficient altitude.
- The maneuver was initiated at an altitude approximately 20% lower than that used in previous successful maneuvers, leaving no margin for error.
- The aircraft's mechanical condition and maintenance records were found to be in good order, with no evidence of mechanical failure contributing to the crash.