Takeoff Aborted After False Stall Warning on Runway 28L

Casualties unknown • Boise, ID, US

A flight was cleared for takeoff after a gate delay, but the stickshaker activated shortly after rotation speed was called. The crew aborted the takeoff and stopped in the overrun with no injuries or significant damage.

What happened

Following a gate delay caused by late-arriving passengers, the flight received clearance for departure on runway 28L. Approximately four seconds after the pilot announced rotation speed, the stickshaker activated, prompting an immediate abort of the takeoff. Cockpit voice recorder data indicated that the thrust reversers were deployed eleven seconds later. The aircraft was brought to a halt in the dirt overrun, coming to rest approximately fifty feet past the end of the runway.

The investigation

The aircraft had been dispatched from Seattle, WA, with an inoperative anti-skid system, properly placarded for this condition. A subsequent examination revealed that the right flap position transmitter had malfunctioned due to corrosion. This component failure is critical because a malfunction of either flap position transmitter can send an erroneous flap setting signal to the stall warning computer.

Findings

The erroneous signal from the faulty transmitter caused the stall warning computer to activate the stickshaker and stall warning system at incorrect airspeeds during the takeoff roll. Despite the alarming warning, only minor damage was sustained by the aircraft, and there were no injuries among those on board.

Safety message

This incident highlights how a single component failure in the flap position sensing system can trigger false stall warnings, potentially leading to unnecessary aborts or confusion during critical phases of flight.

Probable cause

A malfunction of the right flap position transmitter due to corrosion, which sent an erroneous signal to the stall warning computer, activating the stickshaker at incorrect airspeeds.

Frequently asked questions

What happened in the 1982-07-05 Douglas DC-9-31 accident near Boise, ID?

A flight was cleared for takeoff after a gate delay, but the stickshaker activated shortly after rotation speed was called. The crew aborted the takeoff and stopped in the overrun with no injuries or significant damage.

What aircraft was involved and where did it happen?

The accident on 1982-07-05 involved a Douglas DC-9-31, registration N919RW, operated by Republic Airlines West, Inc., at Boise, ID.

What was the probable cause of the accident?

A malfunction of the right flap position transmitter due to corrosion, which sent an erroneous signal to the stall warning computer, activating the stickshaker at incorrect airspeeds.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20020917X04180. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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