Engine Failure During Approach Due to Improper Overhaul

Casualties unknown • Lagrange, GA, US

A pilot lost engine power during cruise flight and attempted an emergency landing on a highway, striking an overpass support column shortly before impact due to inadequate maintenance.

What happened

The aircraft was operating under visual flight rules during daylight hours when the pilot experienced a sudden loss of engine power while in cruise flight. With no immediate airfield available, the pilot maneuvered the aircraft toward Interstate Highway I-85 to execute an emergency landing on the roadway. The attempt ended in a crash when the aircraft struck a support column for an overpass at an altitude of 15 feet above ground level.

The investigation

Records revealed that the engine had undergone an overhaul just 51 hours prior to the accident. Although the overhaul documentation indicated that the magneto had been repaired, and annual inspection records showed compliance with Airworthiness Directive 78-09-07 regarding the magneto, post-crash physical evidence contradicted these claims. Investigators found that neither the carburetor nor the magneto had actually been overhauled.

Further examination of the mechanic involved uncovered a lengthy history of FAA violations for improper repairs. Post-crash testing of the engine components confirmed significant mechanical failures. The left magneto was observed firing intermittently, and the carburetor throttle valve seals were leaking, which induced an excessively lean fuel mixture. Additionally, the carburetor accelerator pump was found to be weak. During a post-crash engine run, the throttle jammed, causing the engine to hesitate, confirming the mechanical deficiencies that led to the power loss.

Findings

The primary contributing factor was the inadequate overhaul of the aircraft engine. The mechanic failed to perform the necessary repairs on the carburetor and magneto despite documentation suggesting otherwise. This lack of proper maintenance resulted in critical component failures, including a leaking throttle valve seal and an intermittent magneto, which directly caused the loss of power during the critical phase of flight.

Safety message

This incident highlights the critical importance of verifying that all required maintenance actions, particularly those mandated by airworthiness directives, are actually performed. Pilots and operators must ensure that mechanics have a clean compliance history and that post-maintenance testing confirms engine reliability before flight.

Probable cause

The pilot's loss of engine power during cruise flight due to inadequate overhaul of the carburetor and magneto by a mechanic with a history of improper repairs, which resulted in a lean mixture and intermittent ignition.

Frequently asked questions

What happened in the 1987-12-06 Piper PA-32-260 accident near Lagrange, GA?

A pilot lost engine power during cruise flight and attempted an emergency landing on a highway, striking an overpass support column shortly before impact due to inadequate maintenance.

What aircraft was involved and where did it happen?

The accident on 1987-12-06 involved a Piper PA-32-260, registration N5587J, at Lagrange, GA.

What was the probable cause of the accident?

The pilot's loss of engine power during cruise flight due to inadequate overhaul of the carburetor and magneto by a mechanic with a history of improper repairs, which resulted in a lean mixture and intermittent ignition.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001213X32650. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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